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Press Release (Feb 25,2012)
Status of TEPCO's Facilities and its services after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (as of 3:00 pm, February 25)
  
Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 
11, 2011, TEPCO's facilities including our nuclear power stations have 
been severely damaged. We deeply apologize for the anxiety and 
inconvenience caused. 
With regard to the accident at Fukushima Daiichi Nuclear Power Station, 
on April 17, 2011, we have compiled the roadmap towards restoration from 
the accident and on July 19 we accomplished the Step1 target "Radiation 
dose is in steady decline". Then on December 16 we confirmed the 
accomplishment of the Step 2 target "Release of radioactive materials is 
under control and radiation doses are being significantly held down". 
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term 
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power 
Units 1-4, TEPCO". 
In addition to the maintenance of the plant's stable condition, we will 
implement Mid-to-Long Term countermeasures towards the decommissioning of 
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to 
their homes as soon as possible and reduce the anxiety of the people in 
Fukushima and the whole nation as soon as possible. 
 
Below is the status of TEPCO's major facilities. 
 
* Updates are underlined. 
 
 [Nuclear Power Station] 
 
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to 
  the earthquake: 
    (Units 4 to 6: outage due to regular inspections before the earthquake) 
 
  - With regard to the water injection volume for Unit 2 reactor, which 
    was increased with temperature figure raising, we have gradually 
    adjusted it to the original volume before temperature increasing 
    (Feed water system: approx. 3.0m3/h, core spray system: approx. 6.0m3/h). 
    During our observing the plant parameter after the decreasing the 
    flow rate of feed water system on February 22, we found that one 
    thermometer in the lower part of the RPV indicated the different 
    movement from others. From 0:21 pm to 2:48 pm on February 23, we 
    investigated the concerned device. As the result of the measurement 
    of DC resistance, we found no breaking wire and availability of the 
    thermometer. But we confirmed that the DC resistance of it became 
    higher than the previous measurement test data. We will evaluate the 
    soundness of the concerned device and examine correspondence in 
    future. We make sure no re-criticality state because there were no 
    significant changes at the monitoring post and as the result of the 
    sampling for the Gas Control System of the Unit 2, we confirmed that 
    the concentration of Xe-135 was below the detectible limit. 
     · At 11:00 am on February 25, the temperature of the lower part of 
       the RPV (top of the lower head)(135°) : approx. 45.0 °C 
     (Reference) 
     · At 11:00 am on February 25, the temperature of the lower part of 
       the RPV (top of the lower head)(270°) : approx. 39.8 °C 
 
  - At 8:30 am Today (Feb. 25), Tepco worker and partner companies' 
    worker found water leakage at welded part of piping at B line of 2nd 
    Cesium adsorption apparatus(SARRY) placed on the 1st floor in 
    Miscellaneous Solid Waste Volume Reduction Treatment Building (High 
    Temperature Incinerator Building) of Fukushima Daiichi Nuclear Power 
    Station. The leakage is just a drop per second and the amount of 
    water leaked is approx. 10 litters (2m x 5m x 1mm). Those leaked 
    water are stayed in barrier in the building and it did not leaked to 
    out of the building. At 10:44 am, we stopped operation of SARRY and 
    closed valve positioned in the upstream of leaked point to prevent 
    further leakage of the water.  We confirmed that the leakage was 
    stopped at 11:10 am. Surface radiation is approx. 4-5mSv/h (2mSv/h in 
    the back ground). We will sample the leaked water and analyze the 
    radioactivity concentration. The treatment of accumulated water is 
    not affected by suspending the SARRY, and there is a lot of purified 
    water that there is no effect injecting water to the reactor. 
    The result of nuclide analysis for leaked water is as follows: 
    I-131: Below detection limit, Cs-134: 1.3 x 105 Bq/cm3, 
    Cs-137: 1.8 x 105 Bq/cm3 
 
  - At 2:09 pm on February 25, we started transfer the accumulated water 
    from the basement of turbine building of Unit 3 to Miscellaneous 
    Solid Waste Volume Reduction Treatment Building (High Temperature 
    Incinerator Building) 
 
· Fukushima Daini Nuclear Power Station: 
    Units 1 to 4: shutdown due to the earthquake 
 
  - Due to checkup of  Process Computer System of Unit 4 (Feb. 14 to 24), 
    we stopped transferring all data of unit 4 to Emergency Response 
    Supporting System (ERSS) according to the plan. However, when the 
    checkup is done on Feb. 24, we had not set the system to restart 
    transferring the data by mistake, so until we restored the system, 
    there were no data transferred to ERSS (The restoration of system was 
    done at 0:57 pm on Feb. 25) 
 
· Kashiwazaki Kariwa Nuclear Power Station: 
    Units 6: under normal operation 
    (Units 1 to 5 and 7: outage due to regular inspections) 
 
 [Thermal Power Station] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Hydro Power Station] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Impacts on Transmission Facilities] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Impacts on Power Supply and Demand Balance] 
This winter, there are some minus factors such as the regular inspection 
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand, 
there are several plus factors such as the recovery of the common thermal 
power stations which suffered the earthquake. As a result, we expect to 
secure 53.7 GW (at the end of February) supply power. 
Compared to the maximum demand in the last winter, which is 51.5 GW, we 
will have 2.2 GW generation reserve margin. 
 
We expect to maintain stable power supply this winter. However, as there 
remains possibilities of unplanned shutdowns at our power stations and 
growth in the demand according to the rapid change in the temperature, we 
would like to ask your reasonable effort to save electricity. 
 
We will continue to make our efforts to maintain stable operation and 
maintenance of the power facilities in order to "prevent in principle" 
the planned blackouts and secure power supply. 
 
 
 
Appendix: Past Progress (As of 3:00 pm on February 25, 2012) (PDF 523KB) 
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB) 
 
* Revised past progress  
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