Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March
11, 2011, TEPCO's facilities including our nuclear power stations have
been severely damaged. We deeply apologize for the anxiety and
inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on
April 17, 2011, we have compiled the roadmap towards restoration from the
accident and on July 19 we accomplished the Step1 target "Radiation dose
is in steady decline". Then on December 16 we confirmed the accomplishment
of the Step 2 target "Release of radioactive materials is under control
and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power
Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will
implement Mid-to-Long Term countermeasures towards the decommissioning of
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to
their homes as soon as possible and reduce the anxiety of the people in
Fukushima and the whole nation as soon as possible.
Below is the status of TEPCO's major facilities.
* Updates are underlined.
[Nuclear Power Station]
·Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to
the earthquake:
(Units 4 to 6: outage due to regular inspections before the earthquake)
* At 10:05 am on February 24, as the change in the injected water amount
was observed, the injected water amount was adjusted from approx. 1.6
m3/h to 2.0m3/h in the feed water system and from approx. 5.2m3/h to 5.0
m3/h in the core spray system.
* At 8:21 am on February 24, as the gradual decline in the treated water
amount was observed in the second Cesium Adsorption Apparatus, its
operation was temporarily suspended to implement the washing of the
filter. At 10:30 am on the same day, the operation was restated and
designed water flow (approx. 36.0m3/h) was achieved at 10:32 am.
* With regard to the water injection volume for Unit 2 reactor, which was
increased with temperature figure raising, we have gradually adjusted it
to the original volume before temperature increasing (Feed water system:
approx. 3.0m3/h, core spray system: approx. 6.0m3/h). During our
observing the plant parameter after decreasing the flow rate of feed
water system on February 22, we found that one thermometer in the lower
part of the RPV (top of the lower head 135°) indicated the different
movement from others. From 0:21 pm to 2:48 pm on February 23, we
investigated the concerned device. As the result of the measurement of
DC resistance, we found no breaking wire and availability of the
thermometer. But we confirmed that the DC resistance of it became higher
than the previous measurement test data. We will evaluate the soundness
of the concerned device and examine correspondence in future. We make
sure no re-criticality state because there were no significant changes
at the monitoring post and as the result of the sampling for the Gas
Control System of the Unit 2, we confirmed that the concentration of
Xe-135 was below the detectible limit.
· At 11:00 am on February 24, the temperature of the lower part of the
RPV (top of the lower head)(135°) : approx. 47.1 °C
(Reference)
· At 11:00 am on February 24, the temperature of the lower part of the
RPV (top of the lower head)(270°) : approx. 38.5 °C
* At 6:00 am on February 24, in order to change the delivery valve of the
pump (A) of the reactor sea water system of Unit 5, we stopped the pump
(C) of the reactor sea water system. As a result, the cooling of the
spent fuel pool was stopped. (the temperature of the spent fuel pool at
the time : approx 17.4°C) At 12:08 pm on the same day, the system was
restarted after the completion of the work. Accordingly the cooling of
the spent fuel pool was restarted as well. (pool temperature at the time
of the cooling restart: approx 18.2°C)
* At 9:40 am on February 24, we started the work to add the flow-meters to
the nitrogen injection line at the side of Primary Containment Vessel of
Unit 1 in order to improve the reliability of nitrogen injection
activity. Due to this work, we suspended the nitrogen injection task
temporarily (*). After the completion of the installation, we restarted
the nitrogen injection. At 1:10 pm, it was confirmed that there was no
significant variation in the parameters.
* In the Chapter 12 of Nuclear Reactor Facilities Security Regulation "The
Way of Ensuring Mid-term Security", as the treatments like "Operational
limitation" or "Measures required in case of not satisfying the
operational limitation" are determined, it is supposed the operator act
per the required measures if it fails to satisfy the operational
limitation. This time, to implement maintenance works, we have suspended
the work of nitrogen injection at the side of Primary Containment Vessel
of Unit 1 by conducting a planned shift beyond the range of operational
limitation (from 9:40 am to 1:10 pm on February 24).
·Fukushima Daini Nuclear Power Station:
Units 1 to 4: shutdown due to the earthquake
·Kashiwazaki Kariwa Nuclear Power Station:
Units 6: under normal operation
(Units 1 to 5 and 7: outage due to regular inspections)
[Thermal Power Station]
·Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Hydro Power Station]
·Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Transmission Facilities]
·Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Power Supply and Demand Balance]
This winter, there are some minus factors such as the regular inspection
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand,
there are several plus factors such as the recovery of the common thermal
power stations which suffered the earthquake. As a result, we expect to
secure 53.7 GW (at the end of February) supply power.
Compared to the maximum demand in the last winter, which is 51.5 GW, we
will have 2.2 GW generation reserve margin.
We expect to maintain stable power supply this winter. However, as there
remains possibilities of unplanned shutdowns at our power stations and
growth in the demand according to the rapid change in the temperature, we
would like to ask your reasonable effort to save electricity.
We will continue to make our efforts to maintain stable operation and
maintenance of the power facilities in order to "prevent in principle" the
planned blackouts and secure power supply.
Appendix: Past Progress (As of 3:00 pm on February 24, 2012) (PDF 711KB)
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB)
* Revised past progress