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Press Release (Feb 24,2012)
Status of TEPCO's Facilities and its services after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (as of 10:00 am, February 24)
  
Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 
11, 2011, TEPCO's facilities including our nuclear power stations have 
been severely damaged. We deeply apologize for the anxiety and 
inconvenience caused. 
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on 
April 17, 2011, we have compiled the roadmap towards restoration from the 
accident and on July 19 we accomplished the Step1 target "Radiation dose 
is in steady decline". Then on December 16 we confirmed the accomplishment 
of the Step 2 target "Release of radioactive materials is under control 
and radiation doses are being significantly held down". 
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term 
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power 
Units 1-4, TEPCO". 
In addition to the maintenance of the plant's stable condition, we will 
implement Mid-to-Long Term countermeasures towards the decommissioning of 
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to 
their homes as soon as possible and reduce the anxiety of the people in 
Fukushima and the whole nation as soon as possible. 
 
Below is the status of TEPCO's major facilities. 
 
* Updates are underlined. 
 
 [Nuclear Power Station] 
 
·Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to 
  the earthquake: 
  (Units 4 to 6: outage due to regular inspections before the earthquake) 
 
* With regard to the water injection volume for Unit 2 reactor, which was 
  increased with temperature figure raising, we have gradually adjusted it 
  to the original volume before temperature increasing (Feed water system: 
  approx. 3.0m3/h, core spray system: approx. 6.0m3/h). During our 
  observing the plant parameter after the decreasing the flow rate of feed 
  water system on February 22, we found that one thermometer in the lower 
  part of the RPV indicated the different movement from others. From 0:21 
  pm to 2:48 pm on February 23, we investigated the concerned device. As 
  the result of the measurement of DC resistance, we found no breaking 
  wire and availability of the thermometer. But we confirmed that the DC 
  resistance of it became higher than the previous measurement test data. 
  We will evaluate the soundness of the concerned device and examine 
  correspondence in future. We make sure no re-criticality state because 
  there were no significant changes at the monitoring post and as the 
  result of the sampling for the Gas Control System of the Unit 2, we 
  confirmed that the concentration of Xe-135 was below the detectible 
  limit. 
  · At 5:00 am on February 24, the temperature of the lower part of the 
    RPV (top of the lower head)(135°) : approx. 48.9 °C (approx. 41.7°C 
    at 5:00 am on February 23) 
  (Reference) 
  · At 5:00 am on February 24, the temperature of the lower part of the 
    RPV (top of the lower head)(270°) : approx. 38.1 °C (approx. 35.9°C 
    at 5:00 am on February 23) 
 
- At 3:11 pm on February 23, in the alternative cooling system of the 
  spent fuel pool of Unit 4, as the inhale pressure of the primary 
  circulating pump showed the tendency of decrease, we stopped the pump in 
  order to conduct flushing of the strainer on its entry side and 
  suspended cooling of the spent fuel pool (the temperature of the pool at 
  the time of the suspension was approx. 25°C) After the flushing, at 5:18 
  pm on the same day we resumed the pump and cooling of the spent fuel 
  pool of Unit 4. (the temperature of the pool at the time of the resuming 
  was approx. 26°C) 
 
- At 6:00 am on February 24, in order to change the delivery valve of the 
  pump (A) of the reactor sea water system of Unit 5, we stopped the pump 
  (C) of the reactor sea water system. As a result, the cooling of the 
  spent fuel pool was stopped. (the temperature of the spent fuel pool at 
  the time : approx 17.4°C) The temperature of the spent fuel pool will 
  increase approx. 0.3°C per hour during the stoppage. 
 
- At 8:21 am on February 24, water flow at the 2nd Cesium adsorption 
  apparatus tends to decrease, so we stopped it to wash the filters device 
  by reversing the water flow. 
 
- At 9:40 am on February 24, we started the work to add the flow-meters to 
  the nitrogen injection line at the side of Primary Containment Vessel of 
  Unit 1 in order to improve the reliability of nitrogen injection 
  activity. Due to this work, we suspended the nitrogen injection task 
  temporarily (*). 
  * In the Chapter 12 of Nuclear Reactor Facilities Security Regulation 
    "The Way of Ensuring Mid-term Security", as the treatments like 
    "Operational limitation" or "Measures required in case of not 
    satisfying the operational limitation" are determined, it is supposed 
    the operator act per the required measures if it fails to satisfy the 
    operational limitation. This time, to implement maintenance works, we 
    have suspended the work of nitrogen injection at the side of Primary 
    Containment Vessel of Unit 1 by conducting a planned shift beyond the 
    range of operational limitation (at 9:40 am on February 24). 
 
·Fukushima Daini Nuclear Power Station: 
    Units 1 to 4: shutdown due to the earthquake 
 
·Kashiwazaki Kariwa Nuclear Power Station: 
    Units 6: under normal operation 
    (Units 1 to 5 and 7: outage due to regular inspections) 
 
 [Thermal Power Station] 
Power supply has returned to normal and the facilities damaged by the 
earthquake are now being handled in a timely manner. 
 
 [Hydro Power Station] 
Power supply has returned to normal and the facilities damaged by the 
earthquake are now being handled in a timely manner. 
 
 [Impacts on Transmission Facilities] 
Power supply has returned to normal and the facilities damaged by the 
earthquake are now being handled in a timely manner. 
 
 [Impacts on Power Supply and Demand Balance] 
This winter, there are some minus factors such as the regular inspection 
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand, 
there are several plus factors such as the recovery of the common thermal 
power stations which suffered the earthquake. As a result, we expect to 
secure 53.7 GW (at the end of February) supply power. 
Compared to the maximum demand in the last winter, which is 51.5 GW, we 
will have 2.2 GW generation reserve margin. 
 
We expect to maintain stable power supply this winter. However, as there 
remains possibilities of unplanned shutdowns at our power stations and 
growth in the demand according to the rapid change in the temperature, we 
would like to ask your reasonable effort to save electricity. 
 
We will continue to make our efforts to maintain stable operation and 
maintenance of the power facilities in order to "prevent in principle" the 
planned blackouts and secure power supply. 
 
 
 
Appendix: Past Progress (As of 10:00 am on February 24, 2012) (PDF 739KB) 
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB) 
 
* Revised past progress 
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