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Corporate Information

 
Press Release (Feb 19,2012)
Status of TEPCO's Facilities and its services after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (as of 11:00 am, February 19)
 Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 
11, 2011, TEPCO's facilities including our nuclear power stations have 
been severely damaged. We deeply apologize for the anxiety and 
inconvenience caused. 
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on 
April 17, 2011, we have compiled the roadmap towards restoration from the 
accident and on July 19 we accomplished the Step1 target "Radiation dose 
is in steady decline". Then on December 16 we confirmed the accomplishment 
of the Step 2 target "Release of radioactive materials is under control 
and radiation doses are being significantly held down". 
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term 
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power 
Units 1-4, TEPCO". 
In addition to the maintenance of the plant's stable condition, we will 
implement Mid-to-Long Term countermeasures towards the decommissioning of 
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to 
their homes as soon as possible and reduce the anxiety of the people in 
Fukushima and the whole nation as soon as possible. 
 
Below is the status of TEPCO's major facilities. 
 
*The updates are underlined 
 
 [Nuclear Power Station] 
 
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to 
  the earthquake: 
  (Units 4 to 6: outage due to regular inspections before the earthquake) 
 
- At 10:00 am on February 18, regarding the accumulated water at the 
  basement of Unit 6 Turbine Building, transfer to the temporary tank 
  started. At 4:00 pm on the same day, the transfer came to a stop. 
 
- At 7:05 am on February 18, within the Unit 2 SFP alternative cooling 
  system, an alarm sounded showing that the water flow difference was 
  large at the gateway of primary system pump and the system automatically 
  shutdown. After that, we confirmed there was no abnormalities such as 
  leakage at the location where the primary system shutdown. However, as 
  temperature decreased in the outer temperature, the secondary system 
  cooing water temperature also decreased and it may freeze, with a view 
  toward facility protection, we resumed it so as to prevent the primary 
  and secondary system from freezing. Upon resumption, we made sure there 
  was no leakage or parameter abnormalities, and by releasing the alarm at 
  11:54 pm on February 18, we activated the system. Since we do not see 
  any abnormalities, operation of the system is still continuing. 
 
- At around 5:00 am on February 8, the alarm which indicates the 
  abnormally low suction pressure of the high pressure RO pump in the 
  desalination apparatus of Unit 2 spent fuel pool went off and the device 
  was automatically shut down. The interlock closed all the isolation 
  valves in the system and the alternative cooling system for the spent 
  fuel pool was activated so there was no interruption to the cooling 
  process. We also confirmed that there was no leakage from the apparatus. 
  Due to the investigation afterwards we assumed that an instantaneous 
  fall in the pressure had caused this shut down. After we confirmed that 
  certain measures have been taken to prevent this we restarted the 
  operation at 3:20 pm of February 18, but at 7:05 pm on the same day 
  another alarm which indicates that the difference of the water flow 
  between the entrance and the exit of the primary line pump of the 
  substitutive cooling system of the spent fuel pool of unit 2 went off 
  and the system shut had down automatically. Due to this the desalting 
  facility has also shut down, but later we reactivated the system and at 
  10:44 on February 19 we restarted the operation of the desalting facility. 
 
- At 9:57 am on February 19, with regard to the water injection volume for 
  Unit 3 reactor, as there was latitude of the current water injection 
  volume against the equivalent decay heat, for the purpose of reducing 
  the transfer and treatment works of the increased accumulated water due 
  to the increase in water injection to Unit 2, we changed the water 
  injection volume by feed water system from approx. 3.0 m3/h to 2.0 m3/h. 
  (The water injection level from reactor core system is continuing at 5.0 
  m3/h.) 
 
- At 10:00 am on February 19, as for the accumulated water at the Unit 6 
  Turbine Building basement, transfer to the temporary tank commenced. 
 
· Fukushima Daini Nuclear Power Station: 
  (Units 1 to 4: shutdown due to the earthquake) 
 
· Kashiwazaki Kariwa Nuclear Power Station: Units 6: under normal 
  operation 
  (Units 1 to 5 and 7: outage due to regular inspections) 
 
 [Thermal Power Station] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Hydro Power Station] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Impacts on Transmission Facilities] 
· Power supply has returned to normal and the facilities damaged by the 
  earthquake are now being handled in a timely manner. 
 
 [Impacts on Power Supply and Demand Balance] 
This winter, there are some minus factors such as the regular inspection 
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand, 
there are several plus factors such as the recovery of the common thermal 
power stations which suffered the earthquake. As a result, we expect to 
secure 53.7 GW (at the end of February) supply power. 
Compared to the maximum demand in the last winter, which is 51.5 GW, we 
will have 2.2 GW generation reserve margin. 
 
We expect to maintain stable power supply this winter. However, as there 
remains possibilities of unplanned shutdowns at our power stations and 
growth in the demand according to the rapid change in the temperature, we 
would like to ask your reasonable effort to save electricity. 
 
We will continue to make our efforts to maintain stable operation and 
maintenance of the power facilities in order to "prevent in principle" the 
planned blackouts and secure power supply. 
 
 
Appendix: Past Progress (As of 11:00 am on February 19, 2012) (PDF 721KB) 
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB) 
 
* Revised past progress  
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