Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March
11, 2011, TEPCO's facilities including our nuclear power stations have been
severely damaged. We deeply apologize for the anxiety and inconvenience
caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on
April 17, 2011, we have compiled the roadmap towards restoration from the
accident and on July 19 we accomplished the Step1 target "Radiation dose is
in steady decline". Then on December 16 we confirmed the accomplishment of
the Step 2 target "Release of radioactive materials is under control and
radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power Units
1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will
implement Mid-to-Long Term countermeasures towards the decommissioning of
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to
their homes as soon as possible and reduce the anxiety of the people in
Fukushima and the whole nation as soon as possible.
Below is the status of TEPCO's major facilities.
* The updates are underlined.
[Nuclear Power Station]
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to
the earthquake:
(Units 4 to 6: outage due to regular inspections before the earthquake)
- Approximately on 9:40 am on February 8, the staff of a partner company
found the water in a temporary tank to the east of Unit 2 Turbine
Building overflowing. At that time we were pumping up the water in the
sub-drain to the temporary pool as a trial, thus on 10:15 am on the same
day we stopped the pump, and the overflow was stopped. Later we
investigated the site and confirmed that there was no water in trenches
nearby, therefore we concluded that the water didn't run into trenches
nor flow out into the sea. We also sampled the water in the tank. The
results of nuclide analyses were Cs-134: 3.4 x 10-1Bq/cm3, Cs-137: 5.2 x
10-1Bq/cm3. These results are the same as those of the water in the
sub-drain sampled today, therefore we concluded that the overflowed water
was the water in the sub-drain. The volume of the water overflowed from
the tank is evaluated as around 16 m3 at maximum.
- At 10:00 am on February 9, we started to transfer the water accumulated
in the basement of Unit 6 Turbine Building to temporary tanks. At 4:00 pm
on the same day, we stopped the transfer, and at10:00 am on February 10,
we resumed the transfer.
- Since 9:50 am on February 10, we have conducted the work to add
flowmeters to the nitrogen injection line at the side of Primary
Containment Vessel of Unit 3 in order to improve the reliability of
nitrogen injection activity. During this period, due to this work, we
suspended the nitrogen injection task temporarily (*).
* In the Chapter 12 of Nuclear Reactor Facilities Security Regulation
"The Way of Ensuring Mid-term Security", as the treatments like
"Operational limitation" or "Measures required in case of not
satisfying the operational limitation" are determined, it is supposed
the operator act per the required measures if it fails to satisfy the
operational limitation. This time, to implement maintenance works, we
have suspended the work of nitrogen injection at the side of Primary
Containment Vessel of Unit 3 by conducting a planned shift beyond the
range of operational limitation (starting at 9:50 am on February 10).
- From February 2, tendency of temperature rise at the bottom of PCV has
been observed. While we increased the water injection to the reactor and
have been monitoring the trend of the temperature, it is still high
around 70°C. On February 6, we sampled the gas by the gas control system
of Unit 2 Primary Containment Vessel. The density of Xenon 135 at the
entrance of the system was below the detection limit. Since it is below
1Bq/cm3, which is the threshold for judging re-criticality, we confirmed
the reactor didn't go re-critical, however, in order to avoid the
possibility of going re-critical being increased as a result of the water
density in the reactor being increased by rapid injection of cold water
is increased, we injected the boric acid into the reactor as a safety
countermeasure from 0:19 am to 3:20 am on February 7, which was before we
increased the volume of the water injection. At 4:24 am on the same day,
we changed the amount of the core spray system injection water from
3.7m3/h to 6.7m3/h (the amount of the continuing feed water system
injection is 6.8m3/h). Currently, the temperature is approx.66.7°C (as of
5 am on February 10). We will monitor the progress continuously.
- As finding of accumulated water containing radioactive materials at the
trench between the Process Main Building and the Miscellaneous Solid
Waste Volume Reduction Treatment Building [High Temperature Incinerator
Building] (December 18, 2011), we started the inspection of other
trenches at the site on January 11, 2012.
As a result of the inspection made on February 9, the location where the
accumulated water was found and the preliminary results of the nuclide
analysis are as follows:
· Inside the duct for telecommunication cables of Unit 5 & 6
I-131: below the detectible limit, Cs-134: below the detectible limit,
Cs-137:7.2x10-2 Bq/ cm3
· Inside the duct for emergency gas treatment piping
I-131: below the detectible limit, Cs-134:4.6x10-1 Bq/ cm3,
Cs-137:6.7x10-1 Bq/ cm3
· Inside the connection duct of Unit 5's chemical tank, inside the trench
for the piping of suppression pool water, inside the duct for common
suppression pool water surge pipe, inside the trench for fire-
extinguishing piping (at the west of Unit 5), inside the trench for
fire-extinguishing piping (at the west of Unit 6), and the inside the
trench of fire-extinguishing piping (at the south of Unit 5), we
confirmed no accumulated water.
- At 8:39 on February 10, 2012, because it has been observed that the
amount of treatment flow of the second Cesium adsorption apparatus
gradually, we suspended temporarily the operation of the apparatus.
- At 8:45 am on February 10, 2012, at the Centralized Radiation Waste
Treatment Facility, we started transferring accumulated water from On-
site Bunker Building to Process Main Building.
- At 2:14 pm on February 7, 2012, we started transferring the accumulated
water from the basement of turbine building of Unit 2 to Centralized
Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume
Reduction Treatment Building [High Temperature Incinerator Building]). We
stopped the transfer at 8:21 am on February 10, 2012.
- At 10:21 am on February 10, 2012, because the decrease of the volume of
injected water to the Unit 1's reactor, we adjusted the injected water
volume from Core Spray System from approx. 1.7 m3/h to approx. 2.0 m3/h
(we have kept the injected water volume from reactor feed water system at
approx. 4.5 m3/h).
- At 10:05 am on February 10, 2012, because the decrease of the volume of
injected water to the Unit 3's reactor, we adjusted the injected water
volume from reactor feed water system from approx. 2.7 m3/h to approx.
3.0m3/h (we have kept the injected water volume from Core Spray System at
approx. 6.0 m3/h).
- At approximately 6:30 pm on February 9, 2012, at Main Anti-Earthquake
Building, we confirmed that data monitoring using temporarily-installed
meters at Unit 1 was disabled. The measurement of plant parameters
including Containment Atmospheric Monitor, Containment vessel pressure,
Drywell HVH temperature, and the water level of the reactor was cancelled.
Later, because it is confirmed that a fuse of the equipment which supply
electricity to the temporarily-installed meters was blown at the central
control center of Unit 1 & 2 and that the power source for the meters wasv
out of order, at 6:15 am on February 10, we replaced the fuse, resulting
in that the plant parameters excluding Containment Vessel pressure and
the water level of the reactor and the others were turned to under
monitoring using Unit 1's temporarily-installed meters. Later, after
switching the power from the power source for meters whose fault wasv
found to the other power source for meters, all the plant parameters
turned to be monitored using the temporarily-installed meters of Unit 1
at 10:55 am on the same day. For reference, while data monitoring using
Unit 1's temporarily-installed meters was disabled, the key parameters in
terms of safety were continued to be monitored using web-cameras and
others inside the Main Anti-Earthquake Building. Because we confirmed
that there have been no significant fluctuation of the parameters, we
concluded that there is no problem in terms of safety.
· Fukushima Daini Nuclear Power Station:
(Units 1 to 4: shutdown due to the earthquake)
· Kashiwazaki Kariwa Nuclear Power Station: Units 6: under normal operation
(Units 1 to 5 and 7: outage due to regular inspections)
[Thermal Power Station]
· Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Hydro Power Station]
· Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Transmission Facilities]
· Power supply has returned to normal and the facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Power Supply and Demand Balance]
This winter, there are some minus factors such as the regular inspection of
Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand,
there are several plus factors such as the recovery of the common thermal
power stations which suffered the earthquake. As a result, we expect to
secure 53.7 GW (at the end of February) supply power.
Compared to the maximum demand in the last winter, which is 51.5 GW, we
will have 2.2 GW generation reserve margin.
We expect to maintain stable power supply this winter, however, as there
remains possibilities of unplanned shutdowns at our power stations and
growth in the demand according to the rapid change in the temperature, we
would like to ask your reasonable effort to save electricity.
We will continue to make our efforts to maintain stable operation and
maintenance of the power facilities in order to "prevent in principle" the
planned blackouts and secure power supply.
Appendix: Past Progress (As of 11:00 am, February 10, 2012) (PDF 419KB)
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB)
* Revised past progress