Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March
11, 2011, TEPCO's facilities including our nuclear power stations have
been severely damaged. We deeply apologize for the anxiety and
inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on
April 17, 2011, we have compiled the roadmap towards restoration from the
accident and on July 19 we accomplished the Step1 target "Radiation dose
is in steady decline". Then on December 16 we confirmed the accomplishment
of the Step 2 target "Release of radioactive materials is under control
and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power
Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will
implement Mid-to-Long Term countermeasures towards the decommissioning of
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to
their homes as soon as possible and reduce the anxiety of the people in
Fukushima and the whole nation as soon as possible.
Below is the status of TEPCO's major facilities.
* The updates are underlined.
[Nuclear Power Station]
·Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to
the earthquake:
(Units 4 to 6: outage due to regular inspections before the earthquake)
- Since February 2, the tendency of temperature has risen at the bottom of
PCV. Thus, at 7:20 pm on February 3, we changed the injection amount
into Unit 2 reactor through feed water system from approx. 2.9 m3/h to
approx. 4.9 m3/h and changed that though reactor core spray system from
approx. 5.8 m3/h to approx. 3.8 m3/h (which means setting them at those
of before flow adjustment on February 1). After that, we have observed
the tendency of temperature at the upper head of the bottom of PCV. The
temperature was around 70.0 °C (approx. 70.3 °C at 11:00 pm on February
5) and in order to prevent further temperature increase, we decided to
increase the amount of water injected to the reactor. At 1:29 pm on
February 6, the water injection volume to the Unit 2 reactor through the
feed water system was changed from approx. 5.8 m3/h to approx. 6.8 m3/h
(the water injection through the reactor core spray system remains
approx. 3.8 m3/h). At this moment, temperature indicates approx. 70.6 °C
(as of 5:00 am on February 6). We will monitor it continuously.
- At 8:05 am on February 5, our employee on patrol confirmed the water
leakage from valve flange in the outdoor fire protection system piping
in Unit 6. Around 8:31 pm, the valve for upper stream was closed and
leakage was stopped. The water leaked was already processed and there
supposed to be no outflow of the water to the sea because there is no
drain located near by.
- At 10:56 pm on February 4, "Abnormal state (low pressures) in suction
pressure of RO high pressure pump" triggered the alarm in the desalting
facility for spent fuel pool of Unit 2, and the facility automatically
stopped. Because all isolation valves of the system have been closed due
to the interlock and the alternative cooling system for spent fuel pool
is continuously operated, it does not affect the cooling for the spent
fuel pool. In addition, as a result of site check, it was confirmed that
any leakage from the facility was not found. At 5:35 pm of February 5,
the operation of the system was resumed and no abnormality was confirmed.
Also, there was no abnormality regarding the RO high pressure pump. We
will monitor it continuously.
- At 8:40 am on February 6, we temporally suspended the second cesium
adsorption apparatus to conduct backwash of the filter since gradual
decrease in the volume of treatment was confirmed.
- At 4:07 am on February 3, we started water transfer from the basement of
turbine building of Unit 2 to Centralized Radiation Waste Treatment
Facility (Miscellaneous Solid Waste Volume Reduction Treatment Building
[High Temperature Incinerator Building]). At 8:47 am on February 6, the
transfer was stopped.
- Regarding the water leakage from Filtrate water supply valve of Unit 3
spent fuel pool cooling system occurred on January 29,we removed the
valve and completed installation of blanking plate, In addition, we are
temporally suspending the secondary cooling tower in order to prevent
overcooling of spent fuel pool alternative cooling facility. Because the
pool temperature began to increase, at 9:55 am on February 6, we
initiated the secondary cooling tower.
- At 10:00 am on February 6, we started water transfer from the basement
of turbine building of Unit 6 to the temporary tank.
·Fukushima Daini Nuclear Power Station:
(Units 1 to 4: shutdown due to the earthquake)
·Kashiwazaki Kariwa Nuclear Power Station: Units 6: under normal
operation
(Units 1 to 5 and 7: outage due to regular inspections)
[Thermal Power Station]
Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Hydro Power Station]
Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Transmission Facilities]
Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Power Supply and Demand Balance]
This winter, there are some minus factors such as the regular inspection
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the other hand,
there are several plus factors such as the recovery of the common thermal
power stations which suffered the earthquake. As a result, we expect to
secure 53.7 GW (at the end of February) supply power.
Compared to the maximum demand in the last winter, which is 51.5 GW, we
will have 2.2 GW generation reserve margin.
We expect to maintain stable power supply this winter, however, as there
remains possibilities of unplanned shutdowns at our power stations and
growth in the demand according to the rapid change in the temperature, we
would like to ask your reasonable effort to save electricity.
We will continue to make our efforts to maintain stable operation and
maintenance of the power facilities in order to "prevent in principle" the
planned blackouts and secure power supply.
Appendix: Past Progress (As of 10:00 am, February 6, 2012) (PDF 608KB)
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB)
* Revised past progress