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Press Release (Jan 27,2012)
Status of TEPCO's Facilities and its services after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (as of 10:00 am, January 27)
Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 
11, 2011, TEPCO's facilities including our nuclear power stations have been 
severely damaged. We deeply apologize for the anxiety and inconvenience 
caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on 
April 17, 2011, we have compiled the roadmap towards restoration from the 
accident and on July 19 we accomplished the Step1 target "Radiation dose 
is in steady decline". Then on December 16 we confirmed the accomplishment 
of the Step 2 target "Release of radioactive materials is under control 
and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term 
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power Units 
1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will 
implement Mid-to-Long Term countermeasures towards the decommissioning of 
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to 
their homes as soon as possible and reduce the anxiety of the people in 
Fukushima and the whole nation as soon as possible.
Below is the status of TEPCO's major facilities.
* The updates are underlined.
[Nuclear Power Station]
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to 
  the earthquake: 
    (Units 1 to 4: shutdown due to the earthquake)
  - At 1:31 pm on January 26, we started injection of hydrazine to the 
    spent fuel pool of Unit 4 through the circulating cooling system. At 
    3:07 pm, we stopped injection of hydrazine.
  - For the reliability enhancement of water injection into the reactor, 
    the water injection line of the reactor water injection pump on the 
    hill is planned to be changed from pressure hose to polyethylene pipe. 
    Therefore, there is the necessity of the temporary stopping of water 
    injection from the reactor water injection pump for it. At 5:10 pm on 
    January 25, regarding the reactor injection from the feed water system 
    at the Unit 2, we changed the injection line from the pump located 
    uphill to the T/B reactor injecting pump. At 9:47 am on January 26, 
    the volume from the feed water system increased from approx. 7.9 m3/h 
    to approx. 8.7 m3/h, and the volume from the reactor core spray system 
    decreased from approx. 1.0 m3/h to 0 m3/h. After finishing switching 
    work of the water injection line from the water injection pump on the 
    hill at 2:51 pm, the injection line from the feed water system was 
    switched from the reactor water injection pump on the hill to the 
    reactor water injection pump in the turbine building at 3:31. At 3:50 
    pm, the volume from the feed water system decreased from approx. 
    8.7 m3/h to approx. 8.0 m3/h, and the volume from the reactor core 
    spray system increased from 0 m3/h to approx. 1.0 m3/h. At 9:43 am on 
    January 27, the volume from the feed water system decreased from approx. 
    8.2 m3/h to approx. 6.9 m3/h, and the volume from the reactor core 
    spray system increased from approx. 0.7 m3/h to approx. 2.0 m3/h.
  - At 9:44 pm on January 26, we started transfer of the accumulated water 
    from the basement of the turbine building of Unit 2 to the Centralized 
    Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume 
    Reduction Treatment Building [High Temperature Incinerator Facility]). 
    At 8:14 am on January 27, we stopped it.
  - At 9:40 pm on January 26, we started transfer of the accumulated water 
    from the basement of the turbine building of Unit 3 to the Centralized 
    Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume 
    Reduction Treatment Building [High Temperature Incinerator Facility]). 
    At 8:10 am on January 27, we stopped it.
  - For the reliability enhancement of water injection into the reactor, 
    the water discharge line of the reactor water injection pump on the 
    hill is planned to be changed from pressure hose to polyethylene pipe. 
    Therefore, there is the necessity of the temporary stopping of water 
    injection from the reactor water injection pump for it. At 11:50 am 
    January 26, the water injection to the reactor of Unit 3 from the feed 
    water injection system was switched from the reactor water injection 
    pump to the reactor water injection pump in the turbine building. At  
    9:14 am on January 27, the volume from the feed water system increased  
    from approx. 8.5 m3/h to approx. 8.9 m3/h, and the volume from the 
    reactor core spray system decreased from approx. 1.0 m3/h to 0 m3/h.
  - Because of the finding of accumulated water included radioactive 
    materials at the trench between the Process Main Building and the 
    Miscellaneous Solid Waste Volume Reduction Treatment Building[High 
    Temperature Incinerator Building](December 18, 2011), we started the 
    inspection of other trenches at the site on January 11.
    As a result of the inspection on January 26, the locations where 
    accumulated water was discovered and the nuclide analysis results are 
    as follows:
    Off-gas piping duct, Unit 1 
        I-131: below measurable limit, Cs-134: 5.5x10-1Bq/cm3, Cs-137: 
               8.9x10-1Bq/cm3 
    Activated Carbon holdup duct, Unit 1 
        I-131: below measurable limit, Cs-134: 1.6x10-1Bq/cm3, Cs-137:  
               2.7x10-1Bq/cm3 
    Main Transformer Cable Duct, Unit 2 
        I-131: below measurable limit, Cs-134: 8.1x10-1Bq/cm3, Cs-137:  
               1.1x100Bq/cm3 
    Connection Duct of Waste Liquid Surge Tank, Unit 2. 
        We confirmed that no accumulated water. 
    Common-use Boiler Trench of Unit 2-3 
        We confirmed that no accumulated water. 
    Main Transformer Cable Duct, Unit 2 
        I-131: below measurable limit, Cs-134: 1.4x100Bq/cm3, Cs-137:  
               1.8x100Bq/cm3
· Fukushima Daini Nuclear Power Station:
    (Units 1 to 4: shutdown due to the earthquake)
· Kashiwazaki Kariwa Nuclear Power Station: Units 6: under normal operation
    (Units 1 to 5 and 7: outage due to regular inspections)
[Thermal Power Station]  
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner.
[Hydro Power Station] 
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner.
[Impacts on Transmission Facilities]  
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner.
[Impacts on Power Supply and Demand Balance] 
This winter, there are some minus factors such as the regular inspection 
of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station*. On the other hand, 
there are several plus factors such as the recovery of the common thermal 
power stations which suffered the earthquake. As a result, we expect to 
secure 54.6 GW (at the end of January), 53.7 GW (at the end of February) 
supply power.  
Compared to the maximum demand in the last winter, which is 51.5 GW, we 
will have 2.2 - 3.1 GW generation reserve margin.
We expect to maintain stable power supply this winter, however, as there 
remains possibilities of unplanned shutdowns at our power stations and 
growth in the demand according to the rapid change in the temperature, we 
would like to ask your reasonable effort to save electricity.
We will continue to make our efforts to maintain stable operation and 
maintenance of the power facilities in order to "prevent in principle" 
the planned blackouts and secure power supply.
* Correction of Description in [Impacts on Power Supply and Demand Balance]
We described,"there will be some minus factors such as the regular 
inspection of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station" in the 
previous press release. However, because Unit 5 of Kashiwazaki-Kariwa 
Nuclear Power Station has already conducted a regular inspection since 
January 25, we revise the previous sentence to "there are some minus 
factors such as the regular inspection of Unit 5 at Kashiwazaki-Kariwa 
Nuclear Power Station". We would like to apologize for the correction 
(February 8, 2012). 
Appendix: Past Progress (As of 10:00 am, January 27, 2012) (PDF 566KB)  
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB)  
 
* Revised past progress 
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