search



Corporate Information

 
Press Release (Jan 21,2012)
Status of TEPCO's Facilities and its services after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (as of 10:00 am, January 21)
Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 
11, 2011, TEPCO's facilities including our nuclear power stations have 
been severely damaged. We deeply apologize for the anxiety and 
inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on 
April 17, 2011, we have compiled the roadmap towards restoration from the 
accident and on July 19 we accomplished the Step1 target "Radiation dose 
is in steady decline". Then on December 16 we confirmed the accomplishment 
of the Step 2 target "Release of radioactive materials is under control 
and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term 
Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power 
Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will 
implement Mid-to-Long Term countermeasures towards the decommissioning of 
Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to 
their homes as soon as possible and reduce the anxiety of the people in 
Fukushima and the whole nation as soon as possible.

Below is the status of TEPCO's major facilities.

* Updates since the previous press release underlined. 
[Nuclear Power Station] 
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due to 
  the earthquake
   (Units 4 to 6: outage due to regular inspections)

 - At 9:42 am on January 19, we started filling water to the condensate 
   storage tank, Unit 3. At 6:00 pm on the same day, we finished filling 
   water. At 9:05 am on January 21, we restarted filling water. 

 - At 3:17 pm on January 20, we started transferring accumulated water 
   from the basement of T/B, Unit 3 to the Central Radioactive Waste 
   Treatment Facility (Miscellaneous Solid Waste Volume Reduction 
   Treatment Building [High Temperature Incinerator Building]). 

 - At 3:23 pm on January 20, we started transferring accumulated water 
   from the basement of T/B, Unit 2 to the Central Radioactive Waste 
   Treatment Facility (Miscellaneous Solid Waste Volume Reduction 
   Treatment Building [High Temperature Incinerator Building]). 
   At 7:02 am on January 21, a worker from the cooperating company found 
   water leakage from the transfer piping at the large equipment hatch, 
   T/B, Unit 4. 
   We checked the work site and observed water leakage from a flange of 
   the piping to a valve unit. Part of water dripped to the floor outside 
   of the valve unit. At 7:48 am on the same date, we stopped the transfer 
   pump for the accumulated water. At 7:55 am, we confirmed that the 
   dripping of water stopped. The water was within the T/B and there was 
   no leakage to outdoor, no leakage to the sea. The volume of water 
   dripped to the floor of T/B was approx 2 liters. The surface dose rate 
   was 0.1mSv/h. We will conduct flushing of the transfer piping for 
   accumulated water, check the flange and repair. 

 - At 3:37 pm on January 20, we started transferring accumulated water 
   from the basement, T/B, Unit 1 to the basement, T/B, Unit 2. 

 - At 10:00 am on January 20, we started transferring accumulated water 
   from the basement, T/B, Unit 6 to temporary tanks. At 4:00 pm on the 
   same date, we stopped the transfer. 

 - We are gradually adjusting the water injection rate to Reactor, Unit 2 
   in order to switch the water injection piping for reactor injection 
   pump on the hill. At 9:55 am on January 21, we adjusted the amount of 
   the water injection from approx. 5.0 m3/h to approx. 6.0 m3/h through 
   the reactor feed water system, from approx. 5.0 m3/h to approx. 4.0 m3/h 
   through the core spray system. 

 - Further to the finding of accumulated water containing radioactive 
   materials at the trench between the Process Main Building and the 
   Miscellaneous Solid Waste Volume Reduction Treatment Building[High 
   Temperature Incinerator Building](December 18, 2011), on January 11, we 
   started the inspection of other trenches within the power station site. 
   The location and nuclide analysis result (a prompt report) of the 
   inspection on January 20 was as below:
      Off-gas piping duct, Unit 3 
      I-131: below detection limit, Cs-134: 3.1 x 101Bq/cm3, 
      Cs-137:4.1 x 101Bq/cm3 

· Fukushima Daini Nuclear Power Station: 
   (Units 1 to 4: shutdown due to the earthquake) 

· Kashiwazaki Kariwa Nuclear Power Station: Units 5, 6: under normal 
  operation
   (Units 1 to 4 and 7: outage due to regular inspections) 
[Thermal Power Station] 
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner. 
[Hydro Power Station] 
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner. 
[Impacts on Transmission Facilities] 
· Power supply has returned to normal and facilities damaged by the 
  earthquake are now being handled in a timely manner. 
[Impacts on Power Supply and Demand Balance] 
This winter, there will be some minus factors such as the regular 
inspection of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the 
other hand, there will be several plus factors such as the recovery of the 
common thermal power stations which suffered the earthquake. As a result, 
we expect to secure 54.6 GW (at the end of January), 53.7 GW (at the end 
of February) supply power. 
Compared to the maximum demand in the last winter, which is 51.5 GW, we 
will have 2.2 - 3.1 GW generation reserve margin.

We expect to maintain stable power supply this winter, however, as there 
remains possibilities of unplanned shutdowns at our power stations and 
growth in the demand according to the rapid change in the temperature, we 
would like to ask your reasonable effort to save electricity.

We will continue to make our efforts to maintain stable operation and 
maintenance of the power facilities in order to "prevent in principle" the 
planned blackouts and secure power supply. 
Appendix: Past Progress (As of 10:00 am, January 21, 2012) (PDF 349KB) 
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB) 

* Revised past progress 
back to page top


to TOP