Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March
11, 2011, TEPCO's facilities including our nuclear power stations have
been severely damaged. We deeply apologize for the anxiety and
inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on
April 17, we have compiled the roadmap towards restoration from the
accident and then we updated the progress status of roadmap considering
the current situation, on July 19. Accomplishment of the Step1 target
"Radiation dose is in steady decline" has been confirmed. On November 17,
we updated the further progress.
By bringing the reactors and spent fuel pools to a stable cooling
condition and mitigating the release of radioactive materials, we will
make every effort to enable evacuees to return to their homes and for all
citizens to be able to secure a sound life.
Below is the status of TEPCO's major facilities.
* Underlined are updates from the previous press release.
[Nuclear Power Station]
· Fukushima Daiichi Nuclear Power Station: Unit 1 to 3: shut down due
to the earthquake
(Units 4 to 6: outage due to regular inspections)
* At 2:00 am on November 27, we confirmed the difference in temperature at
the gateway of the heat exchanger on the primary side of the Unit 3
spent fuel pool alternative cooling equipment was getting small (inlet
temperature: 19.7°C, outlet temperature: 19.0°C). However, as we could
figure out that it did not affect the cooling of the spent fuel pool
immediately, we decided to conduct a field investigation after dawn. At
6:33 am, as a result of the field investigation, we confirmed the main
valve of watering equipment was closed and therefore we opened it and
filled with water for watering. As a result, we could confirm that the
outlet temperature fell down (as of 7:00 am on November 27, inlet
temperature: 20.3°C, outlet temperature: 15.1°C). Considering this
result, it is confirmed that the cause for the difference in temperature
is that the valve was closed down and the cooling water was not supplied.
We will further investigate the reason of the closing down of the valve
(the temperature of the inlet port of the heat exchanger on the primary
side = the temperature of the spent fuel pool).
· Fukushima Daini Nuclear Power Station:
Units 1 to 4: shutdown due to the earthquake
· Kashiwazaki Kariwa Nuclear Power Station: Units 5, 6: under normal
operation
(Units 1 to 4 and 7: outage due to regular inspections)
[Thermal Power Station]
- Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Hydro Power Station]
- Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Transmission Facilities]
- Power supply has returned to normal and facilities damaged by the
earthquake are now being handled in a timely manner.
[Impacts on Power Supply and Demand Balance]
This winter, there will be some minus factors such as the regular
inspection of Unit 5 at Kashiwazaki-Kariwa Nuclear Power Station. On the
other hand, there will be several plus factors such as the recovery of the
common thermal power stations which suffered the earthquake. As a result,
we expect to secure 54.9 GW (at the end of December), 54.6 GW (at the end
of January), 53.7 GW (at the end of February) supply power.
Compared to the maximum demand in the last winter, which is 51.5 GW, we
will have 2.2 - 3.4 GW generation reserve margin.
We expect to maintain stable power supply this winter, however, as there
remains possibilities of unplanned shutdowns at our power stations and
growth in the demand according to the rapid change in the temperature, we
would like to ask your reasonable effort to save electricity.
We will continue to make our efforts to maintain stable operation and
maintenance of the power facilities in order to "prevent in principle"
the planned blackouts and secure power supply.
Appendix: Past Progress (As of 9:00 am, November 27, 2011) (PDF 348KB)
Appendix: Past Progress (From March 11, 2011 to July 31, 2011) (PDF 225KB)
* Revised past progress