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Top > Releases ・ Announcements > Press Releases > Status of TEPCO's Nuclear Power Stations after theTohoku-Chihou-Taiheiyou-Oki Earthquake > 2013 > Status of TEPCO's Nuclear Power Stations after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (Daily Report as of 5:00 PM on September 16)

Status of TEPCO's Nuclear Power Stations after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (Daily Report as of 5:00 PM on September 16)

Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 11, 2011, TEPCO's facilities including our nuclear power stations have been severely damaged. We deeply apologize for the anxiety and inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on April 17, 2011, we have compiled the roadmap towards restoration from the accident and on July 19 we accomplished the Step1 target "Radiation dose is in steady decline". Then on December 16 we confirmed the accomplishment of the Step 2 target "Release of radioactive materials is under control and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will implement Mid-to-Long Term countermeasures towards the decommissioning of Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to their homes as soon as possible and reduce the anxiety of the people in Fukushima and the whole nation as soon as possible.

Below is the status of TEPCO's Fukushima Daiichi Nuclear Power Station.

* The updates are underlined.

[Fukushima Daiichi Nuclear Power Station]
Unit 1 to 4: Abolishment (April 19, 2012)
Unit 5 to 6: Outage due to regular inspections before the earthquake

-Contaminated water transfer from the underground reservoirs was all completed as of July 1. However, we are continuing to take measures to prevent the expansion of contaminated water, and to conduct sampling activities.

<Measures to prevent the expansion of contaminated water>
· Since the decreases of all-β radioactivity densities in the leakage detection holes (at the northeast side of the underground reservoir No.1, the northeast side of the underground reservoir No.2, and the southwest side of the underground reservoir No.3) have been slow, operations to dilute the underground reservoirs No.1-No.3 by transferring filtered water or desalination-system (RO) treated water (the all-β radioactivity density: approx. 1×101Bq/cm3) into these reservoirs have been conducted as appropriate.

<Recent dilution operations>
· Underground reservoir No.1 (since June 19): On August 3, approx. 60m3 of filtered water was injected.
· Underground reservoir No.2 (since June 27): On August 1, approx. 60m3 of filtered water was injected.
· Underground reservoir No.3 (since July 24): On August 12, approx. 107m3 of water in the drain hole (northeast) of this underground reservoir was injected.

On September 15, leaked water in the leakage detection holes at the underground reservoirs No.1-No.3 was transferred to the temporary aboveground tank, and leaked water in the drain holes at the underground reservoirs No.1 and No.2 was transferred into these underground reservoirs.

<Sampling>
On September 15, sampling was performed in the drain holes of the underground reservoirs No.1-No.7 (14 locations), the leakage detection holes of the underground reservoirs No.1-No.4 and No.6 (sample could not be collected at 2 out of 10 locations), and the observation holes of the underground reservoirs (22 locations). No significant change was found in the analysis results compared to the analysis results on the previous samples (taken on September 14).

-On August 19, puddles were found inside a dike around the H4 area tanks in the power station and outside of a drain valve of the dike.
We found water spread at the bottom level of tanks near Tank No.5 in the Group I in the H4 area. Therefore, we checked the water level of this tank, and found out that the water level has fallen by approx. 3m than the normal level (the amount of water: approx. 300m3). We started collecting the water remaining inside the dike and already collected some of the water. However, since it seemed that the water has flowed out of the dike through the drain valve, we are collecting soil in the surrounding area and continuing to conduct an investigation to find out the range reached by the water. Later, we found streaky traces of flows on the wall surface of a drainage channel located east of the H4 area tanks. The maximum surface dose equivalent rate measured at this location was 6.0mSv/h (γ and β rays (70μm dose equivalent rate)). As this information indicates the possibility that contaminated earth and sand, etc. may have flowed into the drainage channel, we are planning to conduct a detailed investigation and evaluation concerning these traces.

On August 22, transfer of water stored in Tank No.5 in Group I in the H4 area and water collected in a temporary tank (water accumulated inside the dike) into Tank No.10 in Group B in the H4 area was completed.

On August 22, we conducted full inspections (appearance inspections and dose measurement) on the flanged tanks in the other areas, which are of the same type as the tank from which water has leaked. Neither leak nor puddle was found by the appearance inspections on the tanks and the drain valves. However, 2 locations locally showing high dose rates were found around the H3 area tanks. The surfaces of these locations were dry, and we confirmed that there has been no water having flowed into the inside of the dike or the outside of the dike. We also confirmed that the water levels of these tanks remain unchanged after they received water. Additionally, we conducted soundness inspections (visual appearance inspections and water level confirmation) on the flanged tanks that are in use for storage of accumulated water from Units 5 and 6. The inspections were completed on August 26 and showed no abnormality.

During our inspection of Tank No.5 in Group I in the H4 area from which water has leaked, we found out the following:
· 3 tanks including this tank (Tank No.5 in Group I, Tank No.10 in Group I, and Tank No.3 in Group II in the H4 area) were initially installed in the H1 area.
· Ground subsidence occurred in the H1 area at the foundations on which these tanks had been placed, and these tanks were planned to be installed in the H2 area, but actually, have been placed in the H4 area despite our plan.
Although it is still unclear whether there is a causal relationship between the water leaking of Tank No.5 and the tank's having experienced ground subsidence occurred in the H1 area at the foundation on which it had been placed, we conducted water transfer to reduce the risk of leakage.
<The latest transfer operations>
· At 3:57 PM on August 25, transfer from Tank No. 10 in Group I in the H4 area to Tank No. 10 in Group B in the H4 area was started. At 2:07 AM on August 27, the transfer was completed.
· At 10:30 AM on August 29, transfer from Tank No. 3 in Group II in the H4 area to Tank No. 10 in Group B in the H4 area was started. At 11:03 AM on September 2 water transfer was suspended due to the implementation of rainfall countermeasures.

During a patrol on August 31, we found 4 locations showing high dose equivalent rates (β and γ rays (70μm dose equivalent rate)). We consider that there has been no leakage to the outside of the dike because the water levels of all of the relevant tanks have not decreased and also because the drainage valves have been closed.
One of the 4 locations, the connecting pipe section between Tank No.5 and Tank No.6 in Group IV in the H5 area has the heat insulation material placed in the upper part of the pipe, and one drop of water fell to the floor surface when this heat insulation material was pressed. The dose equivalent rate at a location on the floor surface to which the water fell was measured and confirmed to be approx. 230mSv/h. Although water then stopped dropping from the connecting pipe, a discolored part (in a dry condition) of approx. 20cm×20cm was found on the floor surface under the pipe section. Then, we checked the status of water dropping from the connecting pipe between Tank No.5 and Tank No.6 in Group IV in the H5 area with the heat insulation material having been pulled out. Then, we found out that a flange part connecting an isolation valve on the Tank No.5 side (there are 2 isolation valves connecting these tanks and connecting pipe) and the connecting pipe was dripping one drop per approx. 90 seconds. In response, on the same day, we wrapped the adsorption mat around this flange part and covered it with plastic-sheet protection, while placing a drain receiving pan under the flange part on the floor. Both of the 2 isolation valves on the respective Tanks No.5 and No.6 sides of this connecting pipe were found to have been closed. On September 1, we tightened up 12 flange bolts at this flange part, and we confirmed that no water leakage was occurring. For the confirmation purpose, the water levels of Tank No.5 and Tank No.6, in Group IV in the H5 area, were measured and found unchanged.
<Results of the latest patrol>
During a patrol on September 15, no location showed a high dose equivalent rate (β and γ rays (70μm dose equivalent rate)). Locations near the dike floor continued to show low dose equivalent rates since rainwater accumulated inside the dike worked as a shield. Additionally, we conducted a visual inspection, and all of the tanks were found without any abnormality such as leakage (expect for the leaks that resulted in accumulated water inside the dike).

As a result of the full inspections (appearance inspections and dose measurement) conducted on August 22 on the tanks in the areas other than the H4 area, we found tanks (Tank No.4 in Group B and Tank No.10 in Group A, both in the H3 area) each having a part locally showing a high dose rate. Although no water dropping was found on the outside of these tanks, we are planning to transfer water inside the tanks to an RO waste liquid supply tank to reduce the risk of leakage. The transfer is scheduled to be conducted between August 29 and September 17.

Following the leakage from a tank this time, the first sample of water was taken on September 15th at Fukushima Daiichi at the point near the south water outlet (T-2), at the junction of the drainage channels B and C near the H4 area (C-1),at the point of high dose rate measurement in the B drainage channel (B-1), at the point immediately short of the junction with the drainage channel C (B-3), at the point near Fureai Intersection in the drainage channel B (B-0-1), at the point near the main gate in the drainage channel C (C-0), and at the drainage channel C OP. 35m exit (C-2). The second sample was taken at the junction of the drainage channels B and C near the H4 area (C-1), at the point immediately short of the drainage channel C (B-3), at the point near Fureai Intersection in the drainage channel B (B-0-1), at the point near the main gate in the drainage channel C (C-0), at the drainage channel C OP. 35m exit (C-2), and conducted nuclide analysis on the water. The first sample was taken before the effects of the incoming typhoon's rainfall (sampled at the B drainage channel after cleaning of the B drainage channel), and the second sample was taken after the effect of the incoming typhoon's rainfall (after the sandbag outflow at the B drainage channel). Trends will continue to be monitored.

We conducted analysis for, all-β and tritium on water in observation holes (E-1: on the north of the dike that surrounds tanks including Tank No.5 in Group I in the H4 area from which water has leaked, E-2: on the south of the dike that surrounds tanks including Tank No.5 in Group I in the H4 area from which water has leaked) newly installed near the H4 area tanks.

With regards the observation hole (E-1) around the H4 area, tritium in the sample taken on September 14 was detected at 170,000Bq/L, which is increased compared to 150,000Bq/L in the sample taken on September 13 As it is highly possible that the leakage from the H4 area tank and leakage from the desalinization device (reverse osmotic membrane type) at the treated concentrated salt water transfer pipe on March 26 and April 5th, 2012, had an impact on the density, we will continue analysis. With regards the observation hole (E-2) around the H4 area, the analysis from September 14 resulted in a value about the same as that in the sample taken on September 13.
This time, a new analysis was conducted for the observation hole (E-4) around the H4 area. The results of the all-β sample taken on September 15 were 1,300Bq/L, equal to that of E-1. The results of the all-β sample taken on September 15 for E-1 and E-2 were about the same as that in the sample taken on September 14.

· We installed observation holes east of the Unit 1-4 Turbine Buildings, and have been conducting sampling and analysis of groundwater from the observation holes. On June 19, we announced that tritium and strontium were detected at high densities in the observation hole located between Units 1 and 2. Therefore, we have been conducting intensified monitoring and have been pumping up groundwater at the well point and the water collection pit (south) on the east of Unit 1 and Unit 2 Turbine Buildings.

<The latest groundwater transfer operation>
At 3:50 PM on August 31, the water transfer to the Unit 2 vertical shaft C from the well points and the water collection pit (south) was suspended, and the water transfer to the Unit 2 Turbine Building was started at 3:55 PM on August 31.
So that water in the Unit 2 vertical shaft B (water collected due to the closure of the trench) could be transferred to Unit 2 Turbine Building during the daytime from September 3 to 13, groundwater transfer from the well points and the water collection pit (south) was conducted while the transfer destination was sequentially changed. The work of closing the trench was almost completed, and transfer of groundwater in the well points and the water collection pit (south) to Unit 2 Turbine Building has been underway.

<Sampling Results>
The cesium and all-β measurement results taken for the first time on September 13 from groundwater observation holes No. 1-11 on the east side of turbine buildings of Units 1-4 are as follows.

[Groundwater observation holes No. 1-11 measurement results (September 13 sample)]
· Tritium: 85,000Bq/L
· Cesium 134: Less than detection limit (detection limit: 0.36 Bq/L)
· Cesium 137: 0.48 Bq/L
· All-β: 43 Bq/L

* Steam was verified by a camera around 8:00 AM on September 15 around the center area of the 5th floor of the Unit 3 Reactor Building equipment storage pool. No abnormalities were found in monitoring post indicated values or the plant situation, verified by 8:10 AM on the same day (weather data at 8:00 AM: temperature : 24.1℃, humidity: 94.6%). Around 8:00 AM on September 16, steam was no longer verified. No abnormalities were found in the monitoring post indicated values at 8:25 AM (weather data at 8:00 AM: temperature: 25.4℃, humidity: 93.6%).

* When transfer preparations were being conducted from the B area south side weir to prepare for the situation in which rain water from the typhoon drawing close were to accumulate within the weir of the Fukushima Daiichi NPS contaminated water storage tank, around 1:08 PM on September 15 it was verified that the accumulated water from the B area south side weir was overflowing due to sudden rainfall. At 1:13 PM on the same day transfer of the weir accumulated water to a tank in the same area began using the immediately prepared temporary pump, thus stopping the overflow of water. Transfer was halted at 3:22 PM on the same day when the weir accumulated water was almost completely drained.

Analysis results (done by simple measurements1) of all-β radiation within the weir accumulated water of each tank area and the contaminated water storage tank B area (south) are as follows.

· H1 area : 200 Bq/L
· H2 area (north) : 140 Bq/L
· H2 area (south) : 3,700 Bq/L
· H3 area : 4,600 Bq/L
· H4 area (north) : 170,000 Bq/L
· H4 area (east) : 2,400 Bq/L
· H4 area : 110 Bq/L
· H5 area : 430 Bq/L
· H6 area : 160 Bq/L
· H9 area : 9 Bq/L
· H9 area (west) : 8 Bq/L
· B area (north) : 23 Bq/L
· B area (south) : 37 Bq/L
· C area (east) : 24*Bq/L
· C area (west) : 8 Bq/L
· E area : 6 Bq/L
· G 4 area (south) : 3 Bq/L
· G 6 area (north) : 8 Bq/L
· G 6 area (south) : 34 Bq/L

For the weir accumulate water in the H4 area (north) in which high radioactivity was confirmed from all-β radioactivity measurement results (done by simple measurements), water transfer to the same area's tank began around 3:20 PM using a temporary pump, and completed around 11:20 PM the same day.

(1) Simple measurements: A total sample of 500ml taken from 4 areas from each of the weirs. The soaked paper sample is measured using a GM survey meter.

Due to the rainfall in the approaching typhoon, there is the possibility that a large amount of rainfall will accumulate within the weir, the water level will quickly increase and overflow will occur in the contaminated water storage tank C area (east) and C area (west). Radioactive concentration within the weir of the same area (all-β) is 24* Bq/L in C area (east), 8 Bq/L in C area (west), and because it is a lower value than the strontium 90 notice concentration limit (30Bq/L), it could be inferred that the accumulated water within the weir is rainwater. As soon as preparations can be made, as an emergency measure, rainwater accumulated within that weir was drained using a weir drain valve. Due to the rainfall in the approaching typhoon, in the instance in which a large amount of rainfall were to accumulate in other contaminated water storage tank area weirs, should the radioactive concentration (all-β) be lower than the strontium 90 notice concentration limit (30Bq/L), for areas that can be determined to be rainfall, as an emergency measure in order to avoid overflowing of the accumulated rainwater in the weir, drainage should be conducted in the same manner using a weird drain valve.

<Situation as of 2:30 PM, September 16>
· C area (west) : 12:42 PM, drainage begins using weir drain valve
· G 6 area (north) : 1:20 PM, drainage begins using weir drain valve
· E area : 1:30 PM, drainage begins using weir drain valve
· H 9 area : 1:50 PM, drainage begins using weir drain valve
· H 9 area (west) : 1:50 PM, drainage begins using weir drain valve
· C area (east) : 1:50 PM, drainage begins using temporary pump
· G 4 area (south) : 2:20 PM, drainage begins using temporary pump

* It was reported that the value was "2 Bq/L" for the all-β radioactive measurement results (done by simple measurements) in the C area (east), however the correct value was "24 Bq/L." At the time of draining each area's accumulated weir water, even the corrected value (24 Bq/L) is lower than the strontium 90 notice concentration limit (30 Bq/L), thus it is thought that it should have no effect upon the environment.
It was confirmed that the weir accumulate water all-β radioactive measurement results (done by simple measurements) taken on September 16 in the said area were 20 Bq/L.

* Due to the effect of the rainfall of the approaching typhoon, it was verified at 1:30 PM on September 15 that the sandbags (setup with the goal of preventing outflow expansion of H4 area tank leakage water) at the B drainage channel contaminated water storage tank area (at the point immediately short of the drainage channel C) were flowing downstream. Sandbag recovery work was thus conducted at the said areas, and as of 3:20 PM the same day, recovery work was completed. In the morning of September 15, accumulated water in front of sandbags in the B drainage channel was collected using a pump as a typhoon prevention measure.

* At 7:03 AM on September 12, cooling was stopped at the Unit 1 spent fuel pool alternative cooling system due to debris and obstacle removal work. At the time cooling was stopped, the spent fuel cooling pool water temperature was 27.5℃. When all work was completed at 11:10 AM on September 16, the spent fuel pool alternative cooling system was started. There were no abnormalities in the operation condition, and although the temperature rose to 32.0℃ from 27.5℃, there was still a large margin until the upper operation limit of 60℃ and no problems were had with the management of pool water temperature.

* Revised past progress

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