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Top > Releases ・ Announcements > Press Releases > Status of TEPCO's Nuclear Power Stations after theTohoku-Chihou-Taiheiyou-Oki Earthquake > 2013 > Status of TEPCO's Nuclear Power Stations after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (Daily Report as of 3:00 PM on June 19)

Status of TEPCO's Nuclear Power Stations after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (Daily Report as of 3:00 PM on June 19)

Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 11, 2011, TEPCO's facilities including our nuclear power stations have been severely damaged. We deeply apologize for the anxiety and inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on April 17, 2011, we have compiled the roadmap towards restoration from the accident and on July 19 we accomplished the Step1 target "Radiation dose is in steady decline". Then on December 16 we confirmed the accomplishment of the Step 2 target "Release of radioactive materials is under control and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will implement Mid-to-Long Term countermeasures towards the decommissioning of Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to their homes as soon as possible and reduce the anxiety of the people in Fukushima and the whole nation as soon as possible.

Below is the status of TEPCO's Fukushima Daiichi Nuclear Power Station.

* The updates are underlined.

[Fukushima Daiichi Nuclear Power Station]
·Unit 1 to 4: Abolishment (April 19, 2012)
·Unit 5 to 6: Outage due to regular inspections before the earthquake

-As for the underground reservoir No.2 installed within the power station site, 101Bq/cm3 level of radiation was detected as a result of analyzing the water accumulated between the sheet on the outside (bentonite sheet) and the ground (the underground reservoir is made of three layers of impermeable sheets) on April 3. On April 5, radiation was detected in the water between the sheet on the outside (bentonite sheet) and the sheet on the inside (double-layered permeable sheet) as a result of analysis. The radioactivity density of all β detected was approx. 5.9×103Bq/cm3. Considering that there is no drain ditch in the surrounding area, it is considered that there is no possibility of the leaked water flowing into the sea. At 5:10 AM on April 6, the incident was judged to be a leakage which is subject to the application of Article 19-17, Item 10 of the Rule for the Installation, Operation, etc. of Commercial Nuclear Power Reactors (Rule for Commercial Nuclear Power Reactors). The amount of leaked water is approx. 120m3, all γ radioactivity density is approx. 1.5×100Bq/cm3 and all β radioactivity density is approx. 5.9×103Bq/cm3, the γ ray radiation dose leaked is estimated to be approx. 1.8×108Bq and the β radiation dose is estimated to be approx. 7.1×1011Bq. Details are currently being investigated.
While enhancing the monitoring of the water level of the underground reservoir No.3, on April 7, sampling was performed on the water in the drain hole (southwest) and the leakage detection hole (southwest) of the underground reservoir No.3 for the purpose of investigating the leakage location.
Considering that all β nuclides were detected in the water in the leakage detection hole and the drain hole of the underground reservoir No.3 as a result of sampling, it was judged at 8:53 AM on the same day that there may be a small amount of leakage from the impermeable sheet on the outside (bentonite sheet) of the reservoir to the outside.
The samples collected in the morning of April 9 in the drain hole (at 2 locations) and the leakage detection hole (at 2 locations) of the underground reservoir No.1 have been analyzed. As a result, the chloride concentration of the water in the leakage detection hole (northeast) has increased from 4ppm (on the previous day) to 910ppm. At 12:47 PM, water transfer from the underground reservoir No.2 to No.1 utilizing temporary pumps was suspended. Considering that all β nuclides were detected as a result of sampling performed in the leakage detection hole of the underground reservoir No.1 for the purpose of investigating the leakage location, it was judged that there may be a small amount of leakage from the sheet on the inside (double -layer impermeable sheet) to the impermeable sheet on the outside (bentonite sheet) of the reservoir although the water level of the underground reservoir No.1 has not decreased and the analysis results of the drain hole water of the underground No.1 have not yet been confirmed.
On April 10, the soil covering the leakage detection hole (northeast) penetration of the underground reservoir No.2 was removed to perform a visual inspection of the penetration. The removal of the impermeable sheet, gravels, etc. will be continued. Furthermore, drilling work was started for the boring investigation to confirm the contamination condition of the surrounding area of the underground reservoirs and contamination expansion to the sea side. The work will be continued. Though water transfer from the underground reservoir No.3 to No.6 was started at 2:00 PM on the same day, the transfer pump was stopped at 2:03 PM as water leakage from the connection part (flange) of the transfer pump outlet pipe was found. The pipe flange was disassembled for cause investigation. As a result, the cause was identified to be the problem with the flange connection part (inhomogeneous amount of gap on the surfaces). The flange was recovered after replacing the gasket. Since no problem was found as a result of measuring the gaps on other flanges and checking the tightening condition of the flange bolts, the water transfer was started at 9:56 PM on April 12. As for the removal of the soil covering the upper part of the reservoir (embankment) where the leaked water is assumed to have been absorbed, further drilling was performed (a total of the drilling depth: 30-60cm) and the radioactivity density on the ground surface has been reduced down to 0.05mSv/h (β+γ) (max.). At 3:06 PM on April 14, the water transfer from the underground reservoir No.3 to No.6 was suspended as the transfer of the planned water amount had completed.
On April 12, sampling was performed in the drain holes of the underground reservoirs No.1-7 (at 14 locations) and the leakage detection holes of the underground reservoirs No.1-4 and 6 (sample could not be collected at 2 out of 10 locations). As a result, the all β density in the drain hole (northeast) of the underground reservoir No.1 was found to have increased during the period from April 10 to 12. Thus, it was judged that there has been a small amount of leakage from the sheet on the outside (bentonite sheet) to the outside. Since there is no drainage in the surrounding area, there is no possibility that the leaked water has flowed out to the sea.
On April 19, the filtrate water tank No.1 was detached from the transfer line between the buffer tank and the filtrate water tanks No.1/No.2 in order to prepare for the water transfer from the underground reservoir No.1 to the filtrate water tank.

<Measures to prevent the expansion of contaminated water>
On June 18, leaked water in the leakage detection holes at the underground reservoirs No.1-3 and leaked water in the drain holes at the underground reservoir No.2 were transferred to the notch tank.

<Sampling>
On June 18, sampling was performed in the drain holes of the underground reservoirs No.1-7 (14 locations), the leakage detection holes of the underground reservoirs No.1-4 and 6 (sample could not be collected at 2 out of 10 locations), the observation holes of the underground reservoirs (22 locations), the groundwater bypass investigation holes a-c (sample could not be collected at 1 out of 3 locations), the groundwater bypass pump wells No. 1-4, and the observation holes on the sea side (1)-(4). As a result, the all-β density in the leakage detection hole (northeast) of the underground reservoir No.2 showed an increasing trend compared to the previous results (June 17). However, this value is within the range of the past measurement results and no density increase was found in the drain hole (northeast) located on the outside of this leakage detection hole. With the analysis results for the other locations, no significant change was found compared to the analysis results from the sampling performed previously (on June 11 in the groundwater bypass investigation holes a-c, the groundwater bypass pump wells No.1-4, and the observation holes on the sea side (1)-(4), and on June 17 in the other locations). Further, analysis for tritium was performed on water sampled on June 10 and 11 in the groundwater bypass (investigation holes a-c and pump wells No. 1-4; sample could not be collected at 1 investigation hole out of 3 investigation holes) and the observation holes on the sea side (1)-(8), As a result, no significant change was found compared to the previous analysis results.

-At 3:47 PM on June 11, water transfer from the underground reservoir No. 4 (for storage of water accumulated in Units 5 and 6) to F area tanks (temporary tanks) by way of the Unit 6 Turbine Building basement was started. At 4:50 PM on the same day, the transfer was stopped. Please note that water transfer from the underground reservoir No. 4 to the Unit 6 Turbine Building basement is carried out during the daytime using a temporary line.

-At 10:00 AM on June 18, accumulated water transfer from the Unit 6 Turbine Building basement to the temporary tanks was started. The water transfer was suspended at 4:00 PM on the same day, and started at 10:00 AM on June 19.

-At around 11:00 PM on June 15, during dew condensation check, a TEPCO employee found a trace of discolored (brown) water in the leaked water receiving pan under the batch treatment tank (2A) of the multi-nuclide removal equipment system A (currently in trial operation utilizing waste liquid treated at water treatment facility). There is no possibility of water leaking outside the equipment since the trace of water was found in the leaked water receiving pan under the tank. Partially discolored dew condensation water was found attached on the surface of the batch treatment tank (2A), and the partial discoloration was found near the welding line. We therefore placed a bucket to receive the water droplet and have monitored the water dropping condition. Although dew condensation has been continuously occurring on the surface of the tank, no additional dropping of discolored water has been found.
An operation to stop the multi-nuclide removal equipment system A was started at 6:17 PM on June 17, and the system A was stopped at 11:20 PM on the same day.
The results of surface contamination measurement using smear filter paper and radiation dose measurement performed on the surface of the tank and on the floor are as follows.

[Surface contamination measurement using smear filter paper]
- Surface of the batch treatment tank (discolored part near the welding line): 7,900cpm
- Surface of the batch treatment tank (part not discolored near the welding line): 700cpm
- Leaked water receiving pan under the tank (part having trace of discolored water): 4,300cpm
- Leaked water receiving pan under the tank (part not discolored): 1,300cpm
(Reference) Background: 180cpm

[Radiation dose measurement]
- Surface of the batch treatment tank (discolored part near the welding line): Surface radiation dose
γ ray: 0.09mSv/h
β ray + γ ray: 0.18mSv/h
- Surface of the batch treatment tank (part not discolored near the welding line): Surface radiation dose
γ ray: 0.08mSv/h
β ray + γ ray: 0.11mSv/h
- Leaked water receiving pan under the tank (part having trace of discolored water): Surface radiation dose
γ ray: 0.04mSv/h
β ray + γ ray: 0.04mSv/h
- Leaked water receiving pan under the tank (part not discolored): Radiation dose in the atmosphere
γ ray: 0.05mSv/h
β ray + γ ray: 0.06mSv/h

The nuclide analysis results of the dew condensation water (370ml) which was received at a bucket placed under the tank are as follows.

[Nuclide analysis results of water received at the bucket]
- Cs-134: 1.9×100Bq/cm3
- Cs-137: 3.9×100Bq/cm3
- All-β nuclides: 6.7×103Bq/cm3

In the surface contamination measurement using smear filter paper and the radiation dose measurement, the discolored parts showed higher values than the parts not discolored both near the welding line on the surface of the tank and in the leaked water receiving pan. This suggested a possibility of concentrated saltwater, which has been contained in the tank, leaking from the welded part of the tank. Therefore, we were to make detailed investigation.
On June 18, after water was removed from the tank, a liquid penetrant inspection was performed in the surface investigation on the lower part of the tank. As a result, two very narrow holes (pinholes) were found in the welding line where discoloration was found. We will continue the detailed investigation.

-At 9:43 AM on June 19, accumulated water transfer from the Unit 2 Turbine Building basement to the Unit 3 Turbine Building basement was started.

-We installed observation holes east of the Unit 1-4 Turbine Buildings, and have been conducting sampling and analysis of groundwater from the observation holes. On June 19, we announced that tritium and strontium were detected at high densities in the observation hole located between Units 1 and 2, as follows:
- Tritium: 4.6-5.0×105Bq/L (Sampling dates: May 24 and 31, and June 7)
- Strontium-90: 1×103Bq/L (Sampling dates: May 24).
We will continue the sampling and analysis, and conduct intensified monitoring.

* Revised past progress

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