search



Corporate Information

 
Press Release (Sep 02,2012)
Status of TEPCO's Nuclear Power Stations after the Tohoku-Chihou-Taiheiyou-Oki Earthquake (Daily Report as of 3:00 PM, September 2)

Due to the Tohoku-Chihou-Taiheiyou-Oki Earthquake which occurred on March 11, 2011, TEPCO's facilities including our nuclear power stations have been severely damaged. We deeply apologize for the anxiety and inconvenience caused.
With regard to the accident at Fukushima Daiichi Nuclear Power Station, on April 17, 2011, we have compiled the roadmap towards restoration from the accident and on July 19 we accomplished the Step1 target "Radiation dose is in steady decline". Then on December 16 we confirmed the accomplishment of the Step 2 target "Release of radioactive materials is under control and radiation doses are being significantly held down".
In addition, on December 21, 2011, we have compiled the "Mid-to-long-Term Roadmap toward the Decommissioning of Fukushima Daiichi Nuclear Power Units 1-4, TEPCO".
In addition to the maintenance of the plant's stable condition, we will implement Mid-to-Long Term countermeasures towards the decommissioning of Fukushima Daiichi Nuclear Power Units 1-4 to enable evacuees to return to their homes as soon as possible and reduce the anxiety of the people in Fukushima and the whole nation as soon as possible.

Below is the status of TEPCO's nuclear power stations (Fukushima Daiichi and Fukushima Daini).

* The updates are underlined.

[Fukushima Daiichi Nuclear Power Station]
·Unit 1 to 4: Abolishment (April 19, 2012)
·Unit 5 to 6: Outage due to regular inspections before the earthquake

-A worker of TEPCO confirmed that the fluctuation in the amount of water injection for Unit 1 - 3 reactor at 3:00 PM on August 30 at the regular data confirmation.

Unit 1: The amount of water injection from 4.9m3/h (at 2:00 PM) to 4.0m3/h.
(The required amount of water injection was 4.3m3/h.)

Unit 2: The amount of water injection from 7.0m3/h (at 2:00 PM) to 5.5m3/h.
(The required amount of water injection was 6.1m3/h.)

Unit 3: The amount of water injection from 7.0m3/h (at 2:00 PM) to 5.6m3/h.
(The required amount of water injection was 6.1m3/h.)

The shift supervisor judged that the condition did not satisfy the "Operational Requirements"*1 defined by the Technical Specification*2 for Unit 2 at 3:00 PM, for Unit 3 at 3:05 PM and for Unit 1 at 3:07 on the same day. Though we attempted to increase the water injection amounts at the site, the amounts kept decreasing. The water injection amounts were continuously monitored and have been adjusted as below. As a result of site investigation, no water leakage from the reactor injection system was found. In order to check for air intrusion into regular use reactor injection water pump (B) and (C) which were in operation when the injection amounts started decreasing, regular use reactor injection water pump (A) was started at 11:08 PM on the same day and regular use reactor injection water pump (B) was stopped at 11:10 PM. Air vent operation was done on regular use reactor injection water pump (B), and no air intrusion was found as a result. At 11:30 PM, regular use reactor injection water pump (B) was started and regular use reactor injection water pump (C) was stopped at 11:31 PM. Upon conducting air vent operation on regular use reactor injection water pump (C), no air intrusion was found. Since there was a possibility that any dust and foreign material etc. attached to the flow control valve as a cause of the fluctuation in the amount of water injection, we conducted a flushing work on August 31 as follows.

Unit 1: From 7:00 PM to 7:30 PM
Unit 2: From 8:14 PM to 8:27 PM
Unit 3: From 6:00 PM to &:25 PM

We continuously monitored the amount of water injection after the flushing work. Since we confirmed the fluctuation continuously, we adjusted the amount of water injection as follows.
(The required amounts of water injection for each unit were adjusted on September 1 as follows:
Unit 1: 3.8m3/h, Unit 2: 5.4m3/h, Unit 2: 5.4 m3/h )

At 7:14 PM on September 1
[Unit 1] Feed-water system: No change (3.0m3/h), Reactor core spray system: Increased from 1.7m3/h to 2.0m3/h (In total, the amount was increased from 4.7m3/h to 5.0m3/h.)
[Unit 2] Feed-water system: Increased from 1.9m3/h to 2.0m3/h, Reactor core spray system: No change (5.0m3/h) (In total, the amount was increased from 6.9m3/h to 7.0m3/h.)
[Unit 3] Feed-water system: Increased from 2.2m3/h to 2.5m3/h, Reactor core spray system: Increased from 4.3m3/h to 4.5m3/h (In total, the amount was increased from 6.5m3/h to 7.0m3/h.)

At 6:03 AM on September 2
[Unit 1] Feed-water system: Increased from 2.8m3/h to 3.0m3/h, Reactor core spray system: Increased from 1.5m3/h to 2.0m3/h (In total, the amount was increased from 4.3m3/h to 5.0m3/h.)
[Unit 2] Feed-water system: Increased from 1.4m3/h to 2.0m3/h, Reactor core spray system: No change (5.0m3/h) (In total, the amount was increased from 6.4m3/h to 7.0m3/h.)
[Unit 3] Feed-water system: Increased from 2.2m3/h to 2.5m3/h, Reactor core spray system: Increased from 4.2m3/h to 4.5m3/h (In total, the amount was increased from 6.4m3/h to 7.0m3/h.)

At 2:30 PM on September 2, we opened the flow control valve of each unit more widely as part of the cause investigation of the fluctuation, and we started preventing an adhesion of foreign material. For this work, the amounts of water injection of each unit are kept at constant amount due to the retransferring a part of the water which is injected to the reactor to buffer tank.
The cause of this matter will be investigated and the water injection amounts will be continuously monitored. No change has been seen with the bottom of RSV of each unit, and no significant change is found in the monitoring post data.

[ Fukushima Daini Nuclear Power Station ]
·Unit 1 to 4: Shutdown due to the earthquake.

Appendix: Past Progress (As of 3:00 pm, on September 2, 2012) (PDF 608KB)
Appendix: Past Progress (From March 11, 2011 to December 31, 2011) (PDF 523KB)
* Revised past progress

The aforementioned attachments are only available in Japanese.
We apologize for any inconvenience this may cause.
back to page top


to TOP