* Updates from previous press release are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12, 2011. It was assumed to be hydrogen
explosion.
- At 3:37 pm on March 25, 2011, we started injecting freshwater to the
reactor and are now injecting fresh water by a motor driven pump powered
by the off-site transmission line.
- At 10:11 am on December 10, 2011, in addition to water injection from
water feeding system, we started water injection from piping of core
spray system to the reactor.
The current water injection amount from the reactor feed water system is
approx.4.5 m3/h and that from the core spray system is approx.1.9 m3/h.
- At 1:31 am on April 7, 2011, we commenced injection of nitrogen gas into
Primary Containment Vessel.
- At 11:22 am on August 10, 2011, we started cyclic cooling for the water
in the spent fuel pool by an alternative cooling equipment of the Fuel
Pool Cooling and Filtering System.
- On October 28, 2011, we completed installation of the cover for the
Reactor Building in order to contain dispersion of radioactive
substances.
- At 4:04 pm on November 30, 2011, we started operation to inject nitrogen
into the reactor pressure vessel.
- At 6:00 pm on December 19, 2011, a full-scale operation of the PCV gas
management system started.
Unit 2 (Shut down)
- At approximately 6:00 am on March 15, 2011, an abnormal noise began
emanating from nearby Pressure Suppression Chamber and the pressure
within the chamber decreased.
- At 10:10 am on March 26, 2011, we started injecting freshwater to the
reactor and are now injecting fresh water by a motor driven pump powered
by the off-site transmission line.
- At 2:59 pm on September 14, 2011, in addition to water injection from
feed water system, we started water injection from piping of core spray
system to the reactor.
The current water injection amount from the reactor feed water system is
approx.3 m3/h and that from the core spray system is approx.5.9 m3/h.
- With regard to the water injection volume for Unit 2 reactor, which was
increased with temperature figure raising, we have gradually adjusted it
to the original volume before temperature increasing (Feed water system:
approx. 3.0m3/h, core spray system: approx. 6 m3/h). During our
observing the plant parameter after decreasing the flow rate of feed
water system on February 22, we found that one thermometer in the lower
part of the RPV (top of the lower head 135°) indicated the different
movement from others. From 12:21 pm to 2:48 pm on February 23, we
investigated the concerned device. As the result of the measurement of
DC resistance, we found no breaking wire and availability of the
thermometer. But we confirmed that the DC resistance of it became higher
than the previous measurement test data. We will evaluate the soundness
of the concerned device and examine correspondence in future. We make
sure no re-criticality state because there were no significant changes
at the monitoring post and as the result of the sampling for the Gas
Control System of the Unit 2, we confirmed that the concentration of
Xe-135 was below the detectible limit.
·At 11:00 am on February 26, the temperature of the lower part of the
RPV (top of the lower head 135°) : approximate 44.7 °C
(Reference)
·At 11:00 am on February 26, the temperature of the lower part of the
RPV (top of the lower head 270°) : approximate 40.5 °C
- At 5:21 pm on May 31, 2011, we started cyclic cooling for the water in
the spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:06 pm on June 28, 2011, we started injecting nitrogen gas into the
Primary Containment Vessel.
- At 6:00 pm on October 28, 2011, a full operation of the PCV gas control
system started.
- At 10:46 am on December 1, 2011, we started the nitrogen injection to
the Reactor Pressure Vessel.
- At 11:50 am on January 19, 2012, we started the operation of the spent
fuel pool desalting facility.
Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01 am
on March 14, 2011. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, 2011, we started injecting fresh water to the
reactor and are now injecting fresh water by a motor driven pump powered
by the off-site transmission line.
- At 2:58 pm on September 1, 2011, we started water injection by core
spray system in addition to water injection by the reactor feed water
system piping arrangement.
The current water injection amount from the reactor feed water system is
approx. 1.9 m3/h and that from the core spray system is approx. 5.0 m3/h.
- At 7:47 pm on June 30, 2011, we started cyclic cooling for the water in
the spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:01 pm on July 14, 2011, injection of nitrogen gas into the Primary
Containment Vessel started.
- As installation works of the PCV gas control system was completed, we
started a test operation at 11:38 am on February 23, 2012. We confirmed
that an exhaust flow amount was stable at 33 Nm3/h at 2:10 pm and
started an adjustment operation.
- At 4:26 pm on November 30, 2011, we started operation to inject nitrogen
into the reactor pressure vessel.
- At 3:18 pm on January 14, we started operation of the radioactive
material removal instrument for the spent fuel pool.
Unit 4 (Outage due to regular inspection)
- At around 6 am on March 15, 2011, we confirmed the explosive sound and
the sustained damage around the 5th floor rooftop area of Reactor
Building.
- At 12:44 pm on July 31, 2011, we started cyclic cooling for the water in
the spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 10:58 am on November 29, 2011, in order to decrease more salinity, we
installed Ion exchange equipment and started the operation of such
equipment.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, 2011, we started the Residual Heat Removal
System Pump in order to cool the spent fuel pool.
- At 2:45 pm on July 15, 2011, we started the operation of the original
Residual Heat Removal System (System B) by its original seawater pump.
- At 10:11 am on December 22, 2011, since we finished the recovery work of
seawater pump (System B) of equipment water cooling system, we made a
trial run. At 11:25 am on the same day, we confirmed no abnormalities
and restarted the operation.
Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, 2011, we started the Residual Heat Removal
System Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, 2011, we started separately cooling the
reactor through the Residual Heat Removal System and the spent fuel pool
through Equipment Cooling Water System and Fuel Pool Cooling System.
Others
- At around 10:00 am on June 13, 2011, we started the operation of the
circulating seawater purification facility installed at the screen area
of Unit 2 and 3.
- At 8:00 pm on June 17, 2011, we started operation of Water Treatment
Facility against the accumulated water. At 6:00 pm on July 2, we started
the circulating injection cooling to inject the water, which was treated
by the accumulated water treatment system, to the reactors through the
buffer tank.
- At 7:41 pm on August 19, 2011, we started treatment of accumulated water
by parallel operation of one line from the cesium adsorption instrument
to the decontamination instrument and the other treatment line of the
cesium adsorption instrument No.2.
- At 2:06 pm on October 7, 2011, we started to spray purified accumulated
water brought from Unit 5 and 6 continually in order to prevent dust
scattering and potential fire outbreaks from the cut down trees.
- On October 28, 2011, we started installation of the water proof wall at
the sea side, in front of the existing shore protection, Units 1-4, in
order to contain marine pollution by underground water.
- At 12:25 pm on December 13, 2011, we started the re-circulating
operation of desalination facility (reverse osmosis membrane type) for
the purpose of suppression of condensed water after desalination
treatment.
- At 9:18 am on January 31, we started transfer of Sub-drain Water of Unit
6 to the temporary tank. We will conduct transferring to the temporary
tank appropriately.
- From 10:20 am on February 25 to 9:44 am on February 26, we transferred
the accumulated water from the basement of Turbine Building of Unit 1 to
the basement of Turbine Building of Unit 2.
- At 2:09 pm on February 25, we started transfer the accumulated water
from the basement of Turbine Building of Unit 3 to Miscellaneous Solid
Waste Volume Reduction Treatment Building (High Temperature Incinerator
Building).
- From 2:04 pm on February 23, 2012, to 1:51 pm on February 26, we
transferred accumulated water from underground floor of Turbine Building
of Unit 2 to the Process Main Building of the Centralized Radiation
Waste Treatment Facility.
- At 2:04 pm on February 26, we started transfer the accumulated water
from the basement of Turbine Building of Unit 2 to Miscellaneous Solid
Waste Volume Reduction Treatment Building (High Temperature Incinerator
Building).
- At 8:30 am on February 25, Tepco worker and partner companies' worker
found water leakage at welded part of piping at B line of 2nd Cesium
adsorption apparatus placed on the 1st floor in Miscellaneous Solid
Waste Volume Reduction Treatment Building (High Temperature Incinerator
Building) of Fukushima Daiichi Nuclear Power Station. The leakage is
just a drop per second and the amount of water leaked is approx. 10
litters. Those leaked water are stayed in barrier in the building and it
did not leaked to out of the building. At 10:44 am, we stopped operation
of the apparatus and closed valve positioned in the upstream of leaked
point to prevent further leakage of the water. We confirmed that the
leakage was stopped at 11:10 am. Surface radiation is approx. 4-5mSv/h
(2mSv/h in the back ground). We will sample the leaked water and analyze
the radioactivity concentration. The treatment of accumulated water is
not affected by suspending the apparatus, and there is a lot of purified
water that there is no effect injecting water to the reactor.
The result of nuclide analysis for leaked water is as follows:
I-131: Below detection limit, Cs-134: 1.3 x 105 Bq/cm3, Cs-137:
1.8 x 105 Bq/cm3
We isolated the B line of 2nd Cesium adsorption apparatus, with which
the water leakage had been confirmed, and operated the A line of the
apparatus at 6:41 am. At 6:44 pm, the water flow amount reached 20 m3/h,
and the stable treatment of the accumulated water started. At 8:35 am on
February 26, we stopped the A line of the apparatus in order to replace
the pipes and filters of the B line of the apparatus. As the replacement
finished, at 1:31 pm on the same day, we restarted both A and B line of
the apparatus, and the water flow amount reached the rated flow (33.6
m3/h) at 1:50 pm, and the stable treatment of the accumulated water
started.