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Corporate Information

 
Press Release (Feb 09,2012)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 3:00 pm, February 9)
* The updates are underlined 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
- Explosive sound and white smoke were confirmed after the big quake
  occurred at 3:36 pm on March 12, 2011. It was assumed to be hydrogen
  explosion.
- At 3:37 pm on March 25, 2011, we started injecting freshwater to the
  reactor and are now injecting fresh water by a motor driven pump
  powered by the off-site transmission line. 
- At 10:11 am on December 10, 2011, in addition to water injection from
  water feeding system, we started water injection from piping of core
  spray system to the reactor.
  The current water injection amount from the reactor feed water system
  is approx. 4.4 m3/h and that from the core spray system is approx.
  1.8 m3/h.
- At 1:31 am on April 7, 2011, we commenced injection of nitrogen gas
  into Primary Containment Vessel.
- At 11:22 am on August 10, 2011, we started cyclic cooling for the water
  in the spent fuel pool by an alternative cooling equipment of the Fuel
  Pool Cooling and Filtering System.
- On October 28, 2011, we completed installation of the cover for the
  Reactor Building in order to contain dispersion of radioactive
  substances.
- At 4:04 pm on November 30, 2011, we started operation to inject
  nitrogen into the reactor pressure vessel.
- At 6:00 pm on December 19, 2011, a full-scale operation of the PCV gas
  management system started. 
Unit 2 (Shut down) 
- At approximately 6:00 am on March 15, 2011, an abnormal noise began
  emanating from nearby Pressure Suppression Chamber and the pressure
  within the chamber decreased.
- At 10:10 am on March 26, 2011, we started injecting freshwater to the
  reactor and are now injecting fresh water by a motor driven pump
  powered by the off-site transmission line. 
- At 2:59 pm on September 14, 2011, in addition to water injection from
  feed water system, we started water injection from piping of core spray
  system to the reactor.
  Because the tendency of temperature rise at the bottom of PCV had been
  accelerated since February 2, we increased the amount of water injected
  to the reactor and continued monitoring the tendency of the temperature
  fluctuation. Since the temperature had remained high around 70.0°C, we
  injected boric acid into the reactor as a safety countermeasures
  against the re-criticality from 0:19 am to 3:20 am on February 7, and
  changed the amount of the core spray system injection water from 3.7 m3/h
  to 6.7 m3/h at 4:24 am (the amount of the continuing feed water system
  injection is 6.8 m3/h). Currently, the temperature is approx. 66.8°C (as 
  of 11 am on February 9). We will monitor the progress continuously.
  At 9:47 am February 9, as the amount of water injection decrease, we
  adjusted the volume from the feed water system of reactor Unit 2
  increased from approx. 6.4 m3/h to approx. 6.8 m3/h(the amount of the
  continuing injection from reactor core spray system is approx. 6.8 m3/h.
  The current water injection amount from the reactor feed water system
  is approx. 6.8 m3/h and that from the core spray system is approx.
  6.8 m3/h.
- At 5:21 pm on May 31, 2011, we started cyclic cooling for the water in
  the spent fuel pool by an alternative cooling equipment of the Fuel
  Pool Cooling and Filtering System. 
- At 8:06 pm on June 28, 2011, we started injecting nitrogen gas into the
  Primary Containment Vessel.
- At 6:00 pm on October 28, 2011, a full-scale operation of the PCV gas
  control system started. From 10:21 am to 12:35 pm on February 9, for 
  the reliability improvement of nitrogen injection, we are working for 
  installing additional flow meter to the nitrogen injection line of the 
  Primary Containment Vessel (PCV) of Unit 2. Although we suspended the 
  injection temporarily, there is no significant change of the parameter. 
- At 10:46 am on December 1, 2011, we started the nitrogen injection to
  the Reactor Pressure Vessel.
- At 11:50 am on January 19, 2012, we started the operation of the spent
  fuel pool desalting facility.

  * In the Chapter 12 of Nuclear Reactor Facilities Security Regulation 
   "The Way of Ensuring Mid-term Security", as the treatments like 
   "Operational limitation" or "Measures required in case of not 
   satisfying the operational limitation" are determined, it is supposed 
   the operator act per the required measures if it fails to satisfy the 
   operational limitation. This time, to implement maintenance works, we 
   suspended the nitrogen injection into the PCV of Unit 2 (from 10:21 am 
   on February 9 to 12:35 pm on February 9) by conducting a planned shift 
   beyond the range of operational limitation. 
Unit 3 (Shut down) 
- Explosive sound and white smoke were confirmed at approximately 11:01
  am on March 14, 2011. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, 2011, we started injecting fresh water to the
  reactor and are now injecting fresh water by a motor driven pump
  powered by the off-site transmission line.
- At 2:58 pm on September 1, 2011, we started water injection by core
  spray system in addition to water injection by the reactor feed water
  system piping arrangement.
  The current water injection amount from the reactor feed water system
  is approx. 2.8 m3/h and that from the core spray system is approx.
  5.8 m3/h.
  At 7:47 pm on June 30, 2011, we started cyclic cooling for the water in
  the spent fuel pool by an alternative cooling equipment of the Fuel
  Pool Cooling and Filtering System.
- At 8:01 pm on July 14, 2011, injection of nitrogen gas into the Primary
  Containment Vessel started.
- At 4:26 pm on November 30, 2011, we started operation to inject
  nitrogen into the reactor pressure vessel.
- At 3:18 pm on January 14, we started operation of the radioactive
  material removal instrument for the spent fuel pool in Unit 3 
Unit 4 (Outage due to regular inspection) 
- At around 6 am on March 15, 2011, we confirmed the explosive sound and
  the sustained damage around the 5th floor rooftop area of Reactor
  Building.
- At 12:44 pm on July 31, 2011, we started cyclic cooling for the water
  in the spent fuel pool by an alternative cooling equipment of the Fuel
  Pool Cooling and Filtering System.
- At 10:58 am on November 29, 2011, in order to decrease more salinity,
  we installed Ion exchange equipment and started the operation of such
  equipment.
- At this moment, we don't think there is any reactor coolant leakage
  inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, 2011, we started the Residual Heat Removal
  System Pump in order to cool the spent fuel pool.
- At 2:45 pm on July 15, 2011, we started the operation of the original
  Residual Heat Removal System (System B) by its original seawater pump.
- At 10:11 am on December 22, 2011, since we finished the recovery work
  of seawater pump (System B) of equipment water cooling system, we made
  a trial run. At 11:25 am on the same day, we confirmed no abnormalities
  and restarted the operation.
- At this moment, we don't think there is any reactor coolant leakage
  inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, 2011, we started the Residual Heat Removal
  System Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, 2011, we started separately cooling the
  reactor through the Residual Heat Removal System and the spent fuel
  pool through Equipment Cooling Water System and Fuel Pool Cooling
  System.
- With the regular inspection of the residual heat removal system (RHR) 
  at 10:14 on February 9, we stopped the RHR. At 2:02 pm, we rebooted the 
  system and restarted the reactor cooling. Due to the suspension, the 
  reactor's water temperature increased from 27.5°C to 30.6°C temporarily, 
  but in terms of the increase level of reactor water temperature, we 
  estimated it no problem. 
- At this moment, we do not think there is any reactor coolant leakage
  inside PCV. 
Others 
- At around 10:00 am on June 13, 2011, we started the operation of the
  circulating seawater purification facility installed at the screen area
  of Unit 2 and 3.
- At 8:00 pm on June 17, 2011, we started operation of Water Treatment
  Facility against the accumulated water. At 6:00 pm on July 2, we
  started the circulating injection cooling to inject the water, which
  was treated by the accumulated water treatment system, to the reactors
  through the buffer tank.
- At 7:41 pm on August 19, 2011, we started treatment of accumulated
  water by parallel operation of one line from the cesium adsorption
  instrument to the decontamination instrument and the other treatment
  line of the cesium adsorption instrument No.2.
- At 2:06 pm on October 7, 2011, we started to spray purified accumulated
  water brought from Unit 5 and 6 continually in order to prevent dust
  scattering and potential fire outbreaks from the cut down trees.
- On October 28, 2011, we started installation of the water proof wall at
  the sea side, in front of the existing shore protection, Units 1-4, in
  order to contain marine pollution by underground water.
- At 12:25 pm on December 13, 2011, we started the re-circulating
  operation of desalination facility (reverse osmosis membrane type) for
  the purpose of suppression of condensed water after desalination
  treatment.
- As finding of accumulated water containing radioactive materials at the
  trench between the Process Main Building and the Miscellaneous Solid
  Waste Volume Reduction Treatment Building [High Temperature Incinerator
  Building] (December 18, 2011), we started the inspection of other
  trenches at the site on January 11.
- As a result of the inspection made on February 8, the preliminary
  results of the nuclide analysis and executed place are as follows:
 · Inside the duct for power cables for the Unit 6 water intake
   I-131: below the detectible limit, Cs-134: 1.0×10-1 Bq/cm3,
   Cs-137: 8.3×10-2 Bq/cm3 
 · Inside the trench for the Unit 5 and 6 storm drain pipes 
   I-131: below the detectible limit, Cs-134: 1.7×10-1 Bq/cm3,
   Cs-137: 2.5×10-1 Bq/cm3 
 · Inside the duct for the Unit 5 radioactive fluid pipes
   I-131: below the detectible limit, Cs-134: 8.0×10-2 Bq/cm3,
   Cs-137: 1.3×10-1 Bq/cm3 
 · Inside the duct for the Unit 6 main transformer cables
   I-131: below the detectible limit, Cs-134: 2.8×10-1 Bq/cm3,
   Cs-137: 4.3×10-1 Bq/cm3 
 · Inside the trench for heavy oil pipes (east of Unit 5)
   I-131: below the detectible limit, Cs-134: 2.0×10-1 Bq/cm3,
   Cs-137: 2.8×10-1 Bq/cm3 
- At 9:18 am on January 31, we started transfer of Sub-drain Water of
  Unit 6 to the temporary tank. We will conduct transferring to the
  temporary tank appropriately.
- At 2:14 pm on February 7, 2012, we started transferring the accumulated
  water from the basement of turbine building of Unit 2 to Centralized
  Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume
  Reduction Treatment Building [High Temperature Incinerator Building]).
- From At 10:00 am to 4:00 pm on February 8, 2012, we transferred the
  accumulated water from inside the turbine building of Unit 6 to the
  temporary tank.
- At 10:00 am on February 9, 2012, we started transferring the
  accumulated water from the turbine building of Unit 6 to the temporary
  tank.
- At 7:10 on February 9, a partner company's worker found that one end of 
  a silt fence of Unit 1 screen came off. The silt fences were installed 
  both inside and outside of the screen, and the one which came off was 
  the inside. At 10:30 am we refitted it. We implemented sampling survey 
  of both silt fences everyday and there was no significant change from 
  today's sample which we took before the incident. 
- The newly found water leakage caused by frost after the previous report 
  (at 3:00 pm on February 3) is as follow: 
  Secondary cooling system air fin cooler of the spent fuel pool 
  alternative cooling system of Unit 4(founded at 2:30 pm on February 9). 
  (Filtrate water* : a drop per approx. 1 second) 
  *Filtrate water: water which takes from dam. 
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