search



Corporate Information

 
Press Release (Feb 08,2012)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 10:00 am, February 8)
*The updates are underlined 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
 - Explosive sound and white smoke were confirmed after the big quake 
   occurred at 3:36 pm on March 12, 2011. It was assumed to be hydrogen 
   explosion.
 - At 3:37 pm on March 25, 2011, we started injecting freshwater to the 
   reactor and are now injecting fresh water by a motor driven pump powered 
   by the off-site transmission line. 
 - At 10:11 am on December 10, 2011, in addition to water injection from 
   water feeding system, we started water injection from piping of core 
   spray system to the reactor.
   The current water injection amount from the reactor feed water system is 
   approx.4.4 m3/h and that from the core spray system is approx. 1.9 m3/h.
 - At 1:31 am on April 7, 2011, we commenced injection of nitrogen gas into 
   Primary Containment Vessel.
 - At 11:22 am on August 10, 2011, we started cyclic cooling for the water 
   in the spent fuel pool by an alternative cooling equipment of the Fuel 
   Pool Cooling and Filtering System. 
 - On October 28, 2011, we completed installation of the cover for the 
   Reactor Building in order to contain dispersion of radioactive 
   substances.
 - At 4:04 pm on November 30, 2011, we started operation to inject nitrogen 
   into the reactor pressure vessel.
 - At 6:00 pm on December 19, 2011, a full-scale operation of the PCV gas 
   management system started. 
Unit 2 (Shut down) 
 - At approximately 6:00 am on March 15, 2011, an abnormal noise began 
   emanating from nearby Pressure Suppression Chamber and the pressure 
   within the chamber decreased. 
 - At 10:10 am on March 26, 2011, we started injecting freshwater to the 
   reactor and are now injecting fresh water by a motor driven pump 
   powered by the off-site transmission line. 
 - At 2:59 pm on September 14, 2011, in addition to water injection from 
   feed water system, we started water injection from piping of core spray 
   system to the reactor. 
   Because the tendency of temperature rise at the bottom of PCV had been 
   accelerated since February 2, we increased the amount of water injected 
   to the reactor and continued monitoring the tendency of the temperature 
   fluctuation. Since the temperature had remained high around 70.0 °C, we 
   injected boric acid into the reactor as a safety countermeasures against 
   the re-criticality from 0:19 am to 3:20 am on February 7, and changed 
   the amount of the core spray system injection water from 3.7m3/h to 6.7
   m3/h at 4:24 am (the amount of the continuing feed water system 
   injection is 6.8m3/h). Currently, the temperature is approx. 66.7°C (as 
   of 5 am on February 8). We will monitor the progress continuously.
   The current water injection amount from the reactor feed water system is 
   approx. 6.5 m3/h and that from the core spray system is approx. 6.8 m3/h.
 - At 5:21 pm on May 31, 2011, we started cyclic cooling for the water in 
   the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
   Cooling and Filtering System. 
 - At 8:06 pm on June 28, 2011, we started injecting nitrogen gas into the 
   Primary Containment Vessel.
 - At 6:00 pm on October 28, 2011, a full-scale operation of the PCV gas 
   control system started. 
 - At 10:46 am on December 1, 2011, we started the nitrogen injection to 
   the Reactor Pressure Vessel.
 - At 11:50 am on January 19, 2012, we started the operation of the spent 
   fuel pool desalting facility.
 - At around 5:00 am on February 8, the alarm of "abnormally low suction 
   pressure of the high pressure RO pump" in the desalination apparatus for 
   the Unit 2 spent fuel pool went off, and the its operation was 
   automatically stopped. The interlock arrangement closed all the 
   isolation valves in the system, and the alternative cooling system for 
   the spent fuel pool continues its operation. Therefore, there is no 
   impact on the cooling. We also confirmed by the site investigation that 
   there was no leakage from the apparatus. 
Unit 3 (Shut down) 
 - Explosive sound and white smoke were confirmed at approximately 11:01 am 
   on March 14, 2011. It was assumed to be hydrogen explosion.
 - At 6:02 pm on March 25, 2011, we started injecting fresh water to the 
   reactor and are now injecting fresh water by a motor driven pump powered 
   by the off-site transmission line.
 - At 2:58 pm on September 1, 2011, we started water injection by core 
   spray system in addition to water injection by the reactor feed water 
   system piping arrangement.
   The current water injection amount from the reactor feed water system is 
   approx. 2.9 m3/h and that from the core spray system is approx. 5.8m3/h.
   At 7:47 pm on June 30, 2011, we started cyclic cooling for the water in 
   the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
   Cooling and Filtering System. 
 - At 8:01 pm on July 14, 2011, injection of nitrogen gas into the Primary 
   Containment Vessel started. 
 - At 4:26 pm on November 30, 2011, we started operation to inject nitrogen 
   into the reactor pressure vessel.
 - At 3:18 pm on January 14, we started operation of the radioactive 
   material removal instrument for the spent fuel pool in Unit 3 
Unit 4 (Outage due to regular inspection) 
 - At around 6 am on March 15, 2011, we confirmed the explosive sound and 
   the sustained damage around the 5th floor rooftop area of Reactor 
   Building.
 - At 12:44 pm on July 31, 2011, we started cyclic cooling for the water in 
   the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
   Cooling and Filtering System.
 - At 10:58 am on November 29, 2011, in order to decrease more salinity, we 
   installed Ion exchange equipment and started the operation of such 
   equipment.
 - At this moment, we don't think there is any reactor coolant leakage 
   inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
 - Sufficient level of reactor coolant to ensure safety is maintained.
 - At 5:00 am on March 19, 2011, we started the Residual Heat Removal 
   System Pump in order to cool the spent fuel pool.
 - At 2:45 pm on July 15, 2011, we started the operation of the original 
   Residual Heat Removal System (System B) by its original seawater pump.
 - At 10:11 am on December 22, 2011, since we finished the recovery work of 
   seawater pump (System B) of equipment water cooling system, we made a 
   trial run. At 11:25 am on the same day, we confirmed no abnormalities 
   and restarted the operation.
 - At this moment, we don't think there is any reactor coolant leakage 
   inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
 - Sufficient level of reactor coolant to ensure safety is maintained.
 - At 10:14 pm on March 19, 2011, we started the Residual Heat Removal 
   System Pump of Unit 6 to cool down Spent Fuel Pool.
 - At 2:33 pm on September 15, 2011, we started separately cooling the 
   reactor through the Residual Heat Removal System and the spent fuel pool 
   through Equipment Cooling Water System and Fuel Pool Cooling System.
 - At this moment, we do not think there is any reactor coolant leakage 
   inside PCV. 
Others 
 - At around 10:00 am on June 13, 2011, we started the operation of the 
   circulating seawater purification facility installed at the screen area 
   of Unit 2 and 3.
 - At 8:00 pm on June 17, 2011, we started operation of Water Treatment 
   Facility against the accumulated water. At 6:00 pm on July 2, we started 
   the circulating injection cooling to inject the water, which was treated 
   by the accumulated water treatment system, to the reactors through the 
   buffer tank.
 - At 7:41 pm on August 19, 2011, we started treatment of accumulated water 
   by parallel operation of one line from the cesium adsorption instrument 
   to the decontamination instrument and the other treatment line of the 
   cesium adsorption instrument No.2.
 - At 2:06 pm on October 7, 2011, we started to spray purified accumulated 
   water brought from Unit 5 and 6 continually in order to prevent dust 
   scattering and potential fire outbreaks from the cut down trees.
 - On October 28, 2011, we started installation of the water proof wall at 
   the sea side, in front of the existing shore protection, Units 1-4, in 
   order to contain marine pollution by underground water.
 - At 12:25 pm on December 13, 2011, we started the re-circulating 
   operation of desalination facility (reverse osmosis membrane type) for 
   the purpose of suppression of condensed water after desalination 
   treatment.
 - As finding of accumulated water containing radioactive materials at the 
   trench between the Process Main Building and the Miscellaneous Solid 
   Waste Volume Reduction Treatment Building [High Temperature Incinerator 
   Building] (December 18, 2011), we started the inspection of other 
   trenches at the site on January 11.
   As a result of the inspection made on February 7, the location where the 
   accumulated water was found and the preliminary results of the nuclide 
   analysis are as follows: 
  · Inside the Unit 5 intake power cable duct 
    I-131: below the detectible limit, Cs-134: 1.4x10-1 Bq/ cm3, 
    Cs-137: 2.0x10-1 Bq/ cm3  
  · Inside the Unit 5 seawater piping duct  
    I-131: below the detectible limit, Cs-134:8.2x10-2 Bq/ cm3, 
    Cs-137: 1.1x10-1 Bq/ cm3 
  · Inside the Unit 5 Main transformer cable duct 
    I-131: below the detectible limit, Cs-134:7.3x10-2 Bq/ cm3, 
    Cs-137: 1.3x10-1 Bq/ cm3 
  · Inside the Unit 5 Booster transformer cable duct 
    I-131: below the detectible limit, Cs-134:2.0x10-1 Bq/ cm3, 
    Cs-137:2.9x10-1 Bq/ cm3 
 - At 9:18 am on January 31, we started transfer of Sub-drain Water of Unit 
   6 to the temporary tank. We will conduct transferring to the temporary 
   tank appropriately.
 - At 2:14 pm on February 7, 2012, we started transferring the accumulated 
   water from the basement of turbine building of Unit 2 to Centralized 
   Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume 
   Reduction Treatment Building [High Temperature Incinerator Building]).
 - At 10:00 am on February 8, 2012, we started transferring the accumulated 
   water from inside the turbine building of Unit 6 to the temporary tank. 
back to page top


to TOP