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Corporate Information

 
Press Release (Jan 02,2012)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 4:00 pm, January 2)
*Updates are underlined 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
- Explosive sound and white smoke were confirmed after the big quake 
  occurred at 3:36 pm on March 12, 2011. It was assumed to be hydrogen 
  explosion.
- At 3:37 pm on March 25, 2011, we started injecting freshwater to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line. 
- At 10:11 am on December 10, 2011, in addition to water injection from 
  water feeding system, we started water injection from piping of core 
  spray system to the reactor.
  Current water injection volume is approx. 4.8 m3/h from the reactor feed 
  water system and approx. 2 m3/h from the core spray system.
- At 1:31 am on April 7, 2011, we commenced injection of nitrogen gas into 
  Primary Containment Vessel.
- At 11:22 am on August 10, 2011, we started cyclic cooling for the water 
  in the spent fuel pool by an alternative cooling equipment of the Fuel 
  Pool Cooling and Filtering System. 
- On October 28, 2011, we completed installation of the cover for the 
  Reactor Building in order to contain dispersion of radioactive 
  substances.
- At 4:04 pm on November 30, 2011, we started operation to inject nitrogen 
  into the reactor pressure vessel.
- At 6:00 pm on December 19, 2011, a full-scale operation of the PCV gas 
  management system started. 
Unit 2 (Shut down) 
- At approximately 6:00 am on March 15, 2011, an abnormal noise began 
  emanating from nearby Pressure Suppression Chamber and the pressure 
  within the chamber decreased. 
- At 10:10 am on March 26, 2011, we started injecting freshwater to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line. 
- At 2:59 pm on September 14, 2011, in addition to water injection from 
  water feeding system, we started water injection from piping of core 
  spray system to the reactor.
  Current water injection amount is approx.2 m3/h in feed water system and 
  approx.7 m3/h in corer spray system
- At 5:21 pm on May 31, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 8:06 pm on June 28, 2011, we started injecting nitrogen gas into the 
  Primary Containment Vessel.
- At 6:00 pm on October 28, 2011, we put the gas management system of the 
  reactor containment vessel in operation.
- At 10:46 am on December 1, 2011, we started the nitrogen injection to 
  the Reactor Pressure Vessel. 
Unit 3 (Shut down) 
- Explosive sound and white smoke were confirmed at approximately 11:01 am 
  on March 14, 2011. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, 2011, we started injecting fresh water to the 
  reactor and are now injecting fresh water by a motor driven pump powered 
  by the off-site transmission line.
- At 2:58 pm on September 1, 2011, we started water injection by core 
  spray system in addition to water injection by the reactor feed water 
  system piping arrangement. 
  The current water injection volume is approx 2.9 m3/h from the reactor 
  feed water system and approx. 6 m3/h from the core spray system.
- At 7:47 pm on June 30, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
  Since inlet pressure of the primary circulation pump in the alternative 
  cooling system of the spent fuel pool frequently tended to decrease due 
  to the effect of clogging of the inlet strainer of the pump, the pump 
  was stopped at each time in order to flush the strainer. However, since 
  this tendency is supposed to continue and the temperature of the spent 
  fuel pool is sufficiently low, which is approx. 13.0°C, and there is 
  enough margin from the operational limit value (upper limit) by the 
  safety regulation, which is 65.0°C, we determined to stop the pump by 
  January 4 of 2012 and temporary stop the cooling of spent fuel pool, 
  considering the exposure dose during the flushing.
  At 4:54 pm on December 30, 2011, the pump was stopped. (Temperature of 
  the spent fuel pool was approx. 13.3°C at the time of shutdown.) It is 
  valuated that the temperature rise of the spent fuel pool due to the 
  shutdown of the pump is approx. 5 to 6 degrees for a day. And it is 
  planned that this pump operates for one time in a day to check the 
  temperature of the spent fuel pool during this temporary operation, 
  since December 31, 2011.
- At 8:01 pm on July 14, 2011, injection of nitrogen gas into the Primary 
  Containment Vessel started. 
- At 4:26 pm on November 30, 2011, we started operation to inject nitrogen 
  into the reactor pressure vessel. 
Unit 4 (Outage due to regular inspection) 
- At around 6 am on March 15, 2011, we confirmed the explosive sound and 
  the sustained damage around the 5th floor rooftop area of Reactor 
  Building.
- At 12:44 pm on July 31, 2011, we started cyclic cooling for the water in 
  the spent fuel pool by an alternative cooling equipment of the Fuel Pool 
  Cooling and Filtering System.
- At 10:58 am on November 29, 2011, in order to decrease more salinity, we 
  installed Ion exchange equipment and started the operation of such 
  equipment.
  At approx. 5:30 pm on January 1, 2012, we observed approx. 240 mm 
  decrease in the water level of the skimmer surge tank*1 of Unit 4 spent 
  fuel pool in the three hours between 2:00 pm to 5:00 pm (According to 
  the operation record so far, there had been an approx. 50 mm decrease.). 
  As a result of the site investigation later, we did not observe any 
  leakage around the Unit 4 reactor building, connecting points of primary 
  system pipes of Unit 4 spent fuel pool alternative cooling system, or 
  its installation space. The water temperature of Unit 4 spent fuel pool 
  as of 5:00 pm on January 1 is 23°C (22°C as of 5:00 am on January 2). 
  The spent fuel pool alternative cooling system is still in operation and 
  there is no problem in cooling the reactor. Though the water level of 
  the spent fuel pool is kept stable without any problem, the water level 
  in the skimmer surge tank continues decreasing. Therefore, from 10:27 pm 
  to 11:13 pm on January 1, we filled water in the skimmer surge tank. At 
  present, the water level in the skimmer surge tank keeps decreasing 
  approx. 90mm/hour. We strengthened surveillance on observation of the 
  water level in the skimmer surge tank, increasing the frequency to once 
  in an hour from once in three hours. At present, no leakage is observed 
  outside the building. No significant change is observed in the water 
  level of the accumulated water in the building.
  By further investigation, we confirmed that amount of water that is 
  equivalent to decreased water level of the skimmer surge tank and amount 
  of water that is equivalent to increased water level of the reactor 
  well*2 are almost the same and the water level at reactor well is lower 
  than that of the spent fuel pool. With these facts, we estimate that 
  situation of gate between the reactor well and the spent fuel pool 
  changed and water flow from the spent fuel pool to the reactor well 
  increased made decrease in water flow from the spent fuel pool to the 
  skimmer surge tank, and so decrease in water level at the skimmer surge 
  tank was more than usual. To decrease the difference between the water 
  level of the reactor well and that of the spent fuel pool, we put water 
  into the reactor well from 11:50 am to 11:59 am on January 2. As of 4:00 
  pm, we can not find decrease in the water level of the skimmer surge 
  tank. We will continue surveillance the water level of the skimmer tank. 

  *1 The tank installed in order to receive the water overflows from the 
    spent fuel pool. The water in the spent fuel pool is overflowed into 
    the skimmer surge tank in order to cool the fuel assembly and remove 
    impurities in the water. The water returns to the spent fuel pool 
    after passing through the heat exchanger and the filter.

  *2 The reactor well is the space which contains the reactor pressure 
    vessel and the lid of the reactor containment vessel. During the 
    periodical inspections, the space filled with water and the fuel is 
    changed.

- At this moment, we don't think there is any reactor coolant leakage 
  inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, 2011, we started the Residual Heat Removal 
  System Pump in order to cool the spent fuel pool.
- At 2:45 pm on July 15, 2011, we started the operation of the original 
  Residual Heat Removal System (System B) by its original seawater pump.
- At 10:11 am on December 22, 2011, since we finished the recovery work of 
  seawater pump (System B) of equipment water cooling system, we made a 
  trial run. At 11:25 am on the same day, we confirmed no abnormalities 
  and restarted the operation.
- At this moment, we don't think there is any reactor coolant leakage 
  inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, 2011, we started the Residual Heat Removal 
  System Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, 2011, we started separately cooling the 
  reactor through the Residual Heat Removal System and the spent fuel pool 
  through Equipment Cooling Water System and Fuel Pool Cooling System.
- At this moment, we do not think there is any reactor coolant leakage 
  inside PCV. 
Others 
- At around 10 am on June 13, 2011, we started the operation of the 
  circulating seawater purification facility installed at the screen area 
  of Unit 2 and 3.
- At 8 pm on June 17, 2011, we started operation of Water Treatment 
  Facility against the accumulated water. At 6:00 pm on July 2, we started 
  the circulating injection cooling to inject the water, which was treated 
  by the accumulated water treatment system, to the reactors through the 
  buffer tank.
- At 7:41 pm on August 19, 2011, we started treatment of accumulated water 
  by parallel operation of one line from the cesium adsorption instrument 
  to the decontamination instrument and the other treatment line of the 
  cesium adsorption instrument No.2.
- At 2:06 pm on October 7, 2011, we started to spray purified accumulated 
  water brought from Unit 5 and 6 continually in order to prevent dust 
  scattering and potential fire outbreaks from the cut down trees.
- On October 28, 2011, we started installation of the water proof wall at 
  the sea side, in front of the existing shore protection, Units 1-4, in 
  order to contain marine pollution by underground water.
- At 12:25 pm on December 13, 2011, we started the re-circulating 
  operation of desalination facility (reverse osmosis membrane type) for 
  the purpose of suppression of condensed water after desalination 
  treatment.
- Since December 22, 2011, the atmospheric temperatures at point C of Unit 
  1 Primary Containment Vessel (PCV) monitored by the Containment 
  Atmospheric Monitoring System had risen (the atmospheric temperature of 
  the PCV on December 22 was approx. 38°C, at 7 pm on December 27 was 
  approx. 49°C). The other temperatures had not risen, so we conducted a 
  survey checking the reliability of the meters from 9 am to 10 am on 
  December 28, and we confirmed that there are no problems. From 11:00am 
  to 12:15pm on the same day, we adjusted the volume of Nitrogen injection, 
  from approx. 8 Nm3/h to approx.18 Nm3/h, and emission of the gas 
  management system, from approx. 23 Nm3/h to approx.30 Nm3/h, in order to 
  identify the cause by monitoring the system with the same injection and 
  emission volume as before December 22. The temperature went up to 
  approx. 54.6°C at 6:00 pm on December 28 at its maximum and fell to 
  approx. 43.3°C at 11:00 am on January 2, 2012. Temperatures at other two 
  points also indicated slight increases but are currently in the stable 
  status.
   Point D: (Maximum) approx. 35.8°C at 5:00 pm on December 29, 2011 → 
            approx. 32.6°C at 11:00 am on January 2, 2012. 
   Point E: (Maximum) approx. 40.0°C at 5:00 pm on December 29, 2011 → 
            approx. 35.8°C at 11:00 am on January 2, 2012. 
  We will continuously conduct the survey for the cause of temperature 
  increase and surveillance of the plant.
- At 3:22 pm on December 28, 2011, we started to transfer accumulated 
  water from the basement of turbine building of Unit 2 to the Centralized 
  Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume 
  Reduction Treatment Building [High Temperature Incinerator Building] and 
  the Process Main Building).
- From 2:37 pm on December 30 to 9:58 am on December 31, 2011, we 
  transferred the accumulated water from the basement of turbine building 
  of Unit 3 to the Centralized Radiation Waste Treatment Facility (the 
  Miscellaneous Solid Waste Volume Reduction Treatment Building [High 
  Temperature Incinerator Building] and the Process Main Building). 
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