* Updates are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12. It was assumed to be hydrogen
explosion.
- At 3:37 pm on March 25, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 10:11 am on December 10, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
Current water injection volume is approx. 4.4 m3/h from the reactor
feed water system and approx. 2 m3/h from the core spray system.
- At 1:31 am on April 7, we commenced injection of nitrogen gas into
Primary Containment Vessel.
- At 11:22 am on August 10, we started cyclic cooling for the water in
the spent fuel pool by an alternative cooling equipment of the Fuel
Pool Cooling and Filtering System.
- On October 28, we completed installation of the cover for the Reactor
Building in order to contain dispersion of radioactive substances.
- At 4:04 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
- At 6:00 pm on December 19, a full-scale operation of the PCV gas
management system started.
Unit 2 (Shut down)
- At approximately 6:00 am on March 15, an abnormal noise began emanating
from nearby Pressure Suppression Chamber and the pressure within the
chamber decreased.
- At 10:10 am on March 26, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:59 pm on September 14, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
Current water injection amount is approx.2.0 m3/h in feed water system
and approx.7.0 m3/h in corer spray system
- At 5:21 pm on May 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the
Primary Containment Vessel.
- At 6:00 pm on October 28, we put the gas management system of the
reactor containment vessel in operation.
- At 10:46 am on December 1, we started the nitrogen injection to the
Reactor Pressure Vessel.
Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01
am on March 14. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, we started injecting fresh water to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:58 pm on September 1, we started water injection by core spray
system in addition to water injection by the reactor feed water system
piping arrangement.
The current water injection volume is approx 3 m3/h from the reactor
feed water system and approx. 6 m3/h from the core spray system.
- At 7:47 pm on June 30, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
Since inlet pressure of the primary circulation pump in the alternative
cooling system of the spent fuel pool frequently tended to decrease due
to the effect of clogging of the inlet strainer of the pump, the pump
was stopped at each time in order to flush the strainer. However, since
this tendency is supposed to continue and the temperature of the spent
fuel pool is sufficiently low, which is approx. 13.0°C, and there
is enough margin from the operational limit value (upper limit) by the
safety regulation, which is 65.0°C, we determined to stop the pump
by January 4 of 2012 and temporary stop the cooling of spent fuel pool,
considering the exposure dose during the flushing.
At 4:54 pm on December 30 of 2011, the pump was stopped. (Temperature
of the spent fuel pool was approx. 13.3°C at the time of shutdown.)
It is valuated that the temperature rise of the spent fuel pool due to
the shutdown of the pump is approx. 5 to 6 degrees for a day. And it is
planned that this pump operates for one time in a day to check the
temperature of the spent fuel pool during this temporary operation,
since December 31, 2011.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary
Containment Vessel started.
- At 4:26 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
Unit 4 (Outage due to regular inspection)
- At around 6 am on March 15, we confirmed the explosive sound and the
sustained damage around the 5th floor rooftop area of Reactor Building.
- At 12:44 pm on July 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 10:58 am on November 29, in order to decrease more salinity, we
installed Ion exchange equipment and started the operation of such
equipment.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System
Pump in order to cool the spent fuel pool.
- At 2:45 pm on July 15, we started the operation of the original
Residual Heat Removal System (System B) by its original seawater pump.
- At 10:11 am on December 22, since we finished the recovery work of
seawater pump (System B) of equipment water cooling system, we made a
trial run. At 11:25 am on the same day, we confirmed no abnormalities
and restarted the operation.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System
Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, we started separately cooling the reactor
through the Residual Heat Removal System and the spent fuel pool
through Equipment Cooling Water System and Fuel Pool Cooling System.
- At this moment, we do not think there is any reactor coolant leakage
inside PCV.
Others
- At around 10 am on June 13, we started the operation of the circulating
seawater purification facility installed at the screen area of Unit 2
and 3.
- At 8 pm on June 17, we started operation of Water Treatment Facility
against the accumulated water. At 6:00 pm on July 2, we started the
circulating injection cooling to inject the water, which was treated by
the accumulated water treatment system, to the reactors through the
buffer tank.
- At 7:41 pm on August 19, we started treatment of accumulated water by
parallel operation of one line from the cesium adsorption instrument to
the decontamination instrument and the other treatment line of the
cesium adsorption instrument No.2.
- At 2:06 pm on October 7, we started to spray purified accumulated water
brought from Unit 5 and 6 continually in order to prevent dust
scattering and potential fire outbreaks from the cut down trees.
- On October 28, we started installation of the water proof wall at the
sea side, in front of the existing shore protection, Units 1-4, in
order to contain marine pollution by underground water.
- At 12:25 pm on December 13, we started the re-circulating operation of
desalination facility (reverse osmosis membrane type) for the purpose
of suppression of condensed water after desalination treatment.
- Since December 22, the atmospheric temperatures at point C of Unit 1
Primary Containment Vessel (PCV) monitored by the Containment
Atmospheric Monitoring System had risen (the atmospheric temperature of
the PCV on December 22 was approx. 38°C, at 7 pm on December 27
was approx. 49°C). The other temperatures had not risen, so we
conducted a survey checking the reliability of the meters from 9 am to
10 am on December 28, and we confirmed that there are no problems.
From 11:00am to 12:15pm on the same day, we adjusted the volume of
Nitrogen injection, from approx. 8 Nm3/h to approx.18 Nm3/h, and
emission of the gas management system, from approx. 23 Nm3/h to approx.
30 Nm3/h, in order to identify the cause by monitoring the system with
the same injection and emission volume as before December 22. The
temperature went up to approx. 54.6°C at 6 pm on December 28 at
its maximum and fell to approx. 46.4°C at 5:00 am on December 31.
Temperatures at other two points also indicated slight increases but
are currently in the stable status.
Point D: (Maximum) approx. 35.8°C at 5:00 pm on December 29 →
approx. 33.6°C at 5:00 am on December 31.
Point E: (Maximum) approx. 40.0°C at 5:00 pm on December 29 →
approx. 37.2°C at 5:00 am on December 31.
We will continuously conduct the survey for the cause of temperature
increase and surveillance of the plant.
- At 3:22 pm on December 28, we started to transfer accumulated water
from the basement of turbine building of Unit 2 to the Centralized
Radiation Waste Treatment Facility (Miscellaneous Solid Waste Volume
Reduction Treatment Building [High Temperature Incinerator Building]
and the Process Main Building).
- From 2:37 pm on December 30 to 9:58 am on December 31, we transferred
the accumulated water from the basement of turbine building of Unit 3
to the Centralized Radiation Waste Treatment Facility (the
Miscellaneous Solid Waste Volume Reduction Treatment Building [High
Temperature Incinerator Building] and the Process Main Building).