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Corporate Information

 
Press Release (Dec 22,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 3:30 pm, December 22)
*Updates are underlined. 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
-Explosive sound and white smoke were confirmed after the big quake
 occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line. 
-At 10:11 am on December 10, in addition to water injection from water
 feeding system, we started water injection from piping of core spray
 system to the reactor.
 At 5:05 am of December 21, decrease in water injection was confirmed and
 we adjusted water injection from the reactor feed water system from
 approx 4.3 m3/h to 4.5 m3/h, and water injection from the core spray
 system from approx. 1.8 m3/h to 2.0 m3/h.
 The current water injection volume is approx 4.5 m3/h from the reactor
 feed water system and approx. 2.0 m3/h from the core spray system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at
 1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System. 
-On October 28, we completed installation of the cover for the Reactor
 Building in order to contain dispersion of radioactive substances.
-At 4:04 pm on November 30, we started operation to inject nitrogen into
 the reactor pressure vessel.
-At 6:00 pm on December 19, a full-scale operation of the PCV gas control
 system started.
-On December 22, according to the operational record thus far, we changed 
 the volume of nitrogen into PCV and that of gas emitted from PCV gas 
 control system. At 10:35 am on the same day, we decreased the nitrogen 
 injection amount from approx. 18Nm3/h to approx. 13Nm3/h. In addition, at 
 11:45 am, we confirmed the volume of gas emitted from the gas management 
 system decreased from approx. 30Nm3/h to 26.9Nm3/h. 
Unit 2 (Shut down) 
-At approximately 6:00 am on March 15, an abnormal noise began emanating
 from nearby Pressure Suppression Chamber and the pressure within the
 chamber decreased. 
-At 10:10 am on March 26, we started injecting freshwater to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line. 
-At 2:59 pm on September 14, in addition to water injection from water
 feeding system, we started water injection from piping of core spray
 system to the reactor.
 The current water injection volume is approx. 2.8 m3/h from the reactor
 feed water system and approx. 6 m3/h from the core spray system.
-At 5:21 pm on May 31, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System.
 At 3:03 pm on December 20, we stopped this system due to inspections in
 the flow rate detector of the alternative cooling equipment of the Fuel
 Pool. This is scheduled to last until around 2:00 pm of December 23 and
 during this time we are expecting that the temperature of the spent fuel
 pool will rise by 21°C( temperature at the time the we stopped the
 system: 15.4 °C).
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary
 Containment Vessel.
-At 6:00 pm on October 28, we put the gas management system of the reactor
 containment vessel in operation.
 On December 22, we conducted the sampling of the gas management system. 
 According to our radionuclide analysis, Xe-135 at the entrance of gas 
 management system was below detection limit (1.1x10-1Bq/cm3), and we 
 confirmed that is below the determination criteria for recriticality such 
 as 1Bq/cm3. 
-At 10:46 am on December 1, we started the nitrogen injection to the
 Reactor Pressure Vessel. 
Unit 3 (Shut down) 
-Explosive sound and white smoke were confirmed at approximately 11:01 am
 on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray
 system in addition to water injection by the reactor feed water system
 piping arrangement. 
 The current water injection volume is approx 2.9m3/h from the reactor
 feed water system and approx. 6 m3/h from the core spray system.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System. (From 1:30 pm to 3:15 pm on December 22, we 
 injected hydrazine (corrosion inhibitor)) 
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary
 Containment Vessel started. 
-At 4:26 pm on November 30, we started operation to inject nitrogen into
 the reactor pressure vessel.
-At 9:43 am on December 22, At the Alternative Cooling apparatus of Spent
 Fuel Pool Cooling and Filtering System, since the suction force of
 primary circulating pump decreased, we stopped the pump to conduct
 flushing of entrance-side strainer of primary circulating pump and
 stopped cooling of spent fuel pool. (The temperature of pool is approx.
 13°C when the pump stopped)
 Then, we flushed the strainer so that the suction force recovered. Thus, 
 at 11:06 am on the same day, restarted the pump and began to cool the 
 spent fuel pool. (The temperature of pool is approx. 13°C when the pump 
 restarted) 
Unit 4 (Outage due to regular inspection) 
-At around 6 am on March 15, we confirmed the explosive sound and the
 sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System.
-At 10:58 am on November 29, in order to decrease more salinity, we
 installed Ion exchange equipment and started the operation of such
 equipment.
-At this moment, we don't think there is any reactor coolant leakage
 inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump
 in order to cool the spent fuel pool.
-At 2:45 pm on July 15, we started the operation of the original Residual
 Heat Removal System (System B) by its original seawater pump.
-At 10:11 am on December 22, since we finished the recovery work of 
 seawater pump (System B) of equipment water cooling system, we made a 
 trial run. At 11:25 am on the same day, we confirmed no abnormalities and 
 restarted the operation. 
-At this moment, we don't think there is any reactor coolant leakage
 inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump
 of Unit 6 to cool down Spent Fuel Pool.
-At 2:33 pm on September 15, we started separately cooling the reactor
 through the Residual Heat Removal System and the spent fuel pool through
 Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage 
 inside PCV. 
Others 
-At around 10 am on June 13, we started the operation of the circulating
 seawater purification facility installed at the screen area of Unit 2 and
 3.
-At 8 pm on June 17, we started operation of Water Treatment Facility
 against the accumulated water. At 6:00 pm on July 2, we started the
 circulating injection cooling to inject the water, which was treated by
 the accumulated water treatment system, to the reactors through the
 buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by
 parallel operation of one line from the cesium adsorption instrument to
 the decontamination instrument and the other treatment line of the cesium
 adsorption instrument No.2. 
-At 2:06 pm on October 7, we started to spray purified accumulated water
 brought from Unit 5 and 6 continually in order to prevent dust scattering
 and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea
 side, in front of the existing shore protection, Units 1-4, in order to
 contain marine pollution by underground water.
-At 12:25 pm on December 13, we started the re-circulating operation of
 desalination facility (reverse osmosis membrane type) for the purpose of
 suppression of condensed water after desalination treatment.
-At 1:57 pm on December 21, transfer of accumulated water was started from
 Unit 2 turbine building to the Centralized Radiation Waste Treatment
 Facility (Miscellaneous Solid Waste Volume Reduction Treatment Building
 [High Temperature Incinerator Building] and Process Main Building).
-At around 1:40 am on December 21, the alarm went off at the desalination
 facility (reverse osmosis membrane type) 2-2 which showed that the
 closing of the backwash water drain valve of the multimedia filter was
 not conducted within the designated time, which led to an automatic
 shutdown of the unit. We confirmed at the site that there was no water
 leak. Since we have enough desalinated water this will not influence the
 water injection. Desalination facility (reverse osmosis membrane type) 3
 can be activated. Then, as the result of valve activity confirmation
 investigation, there is no fault in the facilities. Therefore, we
 considered the phenomenon is transient. At around 10:20 am on the same
 day, we restarted the unit. We will continue to monitor operation status.
-At 10:00 am on December 22, we started to replace the transmission parts 
 of monitoring post No.2 and No.8 which monitor dose rate inside the site. 
 At 11:40 on the same date, we finished the replacement work. In addition, 
 monitoring post No.8 data was unavailable from 11:10 am to 11:40 am, but 
 we confirmed that the other monitoring posts didn't indicate unusual 
 values. Monitoring post No.2 was available during the replacement work 
 due to the replacement parts are different from Monitoring post No.8. 
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