*Updates are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- At 3:37 pm on March 25, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 10:11 am on December 10, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
The current water injection volume is approx 4.7 m3/h from the reactor
feed water system and approx. 2.0 m3/h from the core spray system.
- We commenced injection of nitrogen gas into Primary Containment Vessel
at 1:31 am on April 7.
- At 11:22 am on August 10, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- On October 28, we completed installation of the cover for the Reactor
Building in order to contain dispersion of radioactive substances.
- At 4:04 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
- Since the monitoring results of the decontamination of radioactivity
material and hydrogen density at the Primary Containment Vessel (PCV)
gas controlling system which was in a test run was stable, we started
regular operation of this system at 6:00 pm of December 19.
Unit 2 (Shut down)
- At approximately 6:00 am on March 15, an abnormal noise began emanating
from nearby Pressure Suppression Chamber and the pressure within the
chamber decreased.
- At 10:10 am on March 26, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:59 pm on September 14, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
The current water injection volume is approx. 2.9 m3/h from the reactor
feed water system and approx. 6 m3/h from the core spray system.
- At 5:21 pm on May 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 3:06 am on December 19 and 5:04 am on December 20, the alarm went off
which showed that the flow rates at the inlet and the outlet of the
primary system pump of the Fuel Pool Cooling and Filtering System was
substantially different. We confirmed the site and recognized no leak of
water. Later we implemented a vibration experiment on the
instrumentation piping and confirmed that the alarm had stopped. The
Fuel Pool Cooling and Filtering System has been in normal operation and
there is no problem in cooling.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the
Primary Containment Vessel.
- At 6:00 pm on October 28, we put the gas management system of the
reactor containment vessel in operation.
- At 10:46 am on December 1, we started the nitrogen injection to the
Reactor Pressure Vessel.
Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01 am
on March 14. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, we started injecting fresh water to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:58 pm on September 1, we started water injection by core spray
system in addition to water injection by the reactor feed water system
piping arrangement.
The current water injection volume is approx 2.8 m3/h from the reactor
feed water system and approx. 5.9 m3/h from the core spray system.
- At 7:47 pm on June 30, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary
Containment Vessel started.
- At 4:26 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
Unit 4 (Outage due to regular inspection)
- At around 6 am on March 15, we confirmed the explosive sound and the
sustained damage around the 5th floor rooftop area of Reactor Building.
- At 12:44 pm on July 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 10:58 am on November 29, in order to decrease more salinity, we
installed Ion exchange equipment and started the operation of such
equipment.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System Pump
in order to cool the spent fuel pool.
- At 2:45 pm on July 15, we started the operation of the original Residual
Heat Removal System (System B) by its original seawater pump.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System
Pump of Unit 6 to cool down Spent Fuel Pool.
- At 2:33 pm on September 15, we started separately cooling the reactor
through the Residual Heat Removal System and the spent fuel pool through
Equipment Cooling Water System and Fuel Pool Cooling System.
- At this moment, we do not think there is any reactor coolant leakage
inside PCV.
Others
- At around 10 am on June 13, we started the operation of the circulating
seawater purification facility installed at the screen area of Unit 2
and 3.
- At 8 pm on June 17, we started operation of Water Treatment Facility
against the accumulated water. At 6:00 pm on July 2, we started the
circulating injection cooling to inject the water, which was treated by
the accumulated water treatment system, to the reactors through the
buffer tank.
- At 7:41 pm on August 19, we started treatment of accumulated water by
parallel operation of one line from the cesium adsorption instrument to
the decontamination instrument and the other treatment line of the
cesium adsorption instrument No.2.
- At 2:06 pm on October 7, we started to spray purified accumulated water
brought from Unit 5 and 6 continually in order to prevent dust
scattering and potential fire outbreaks from the cut down trees.
- On October 28, we started installation of the water proof wall at the
sea side, in front of the existing shore protection, Units 1-4, in order
to contain marine pollution by underground water.
- At 12:25 pm on December 13, we started the re-circulating operation of
desalination facility (reverse osmosis membrane type) for the purpose of
suppression of condensed water after desalination treatment.
- On December 19 an employee of TEPCO who had engaged in repair works at
Fukushima Daiichi Stabilizing centre was diagnosed as infected by Noro
virus. Other than the two workers that have been diagnosed as infected
by Noro virus so far, another TEPCO employee who had engaged in works at
the Fukushima Daiichi Power Plant was diagnosed as Gastroenteritis
caused by a virus. We disinfected the working office of the two TEPCO
employees. We plan to inform persons/parties concerned of fundamental
matters such as strict enforcement of washing hands and gargling,
re-enforcement of disinfecting ways in case of onset, a medical team
responding system etc.
- At 8:58 am on December 20 we stopped the Cesium adsorption apparatus in
order to adjust the water level of each turbine building and the
Centralized Radiation Waste Treatment Facility (Miscellaneous Solid
Waste compressing building [high temperature incinerator building] and
Process Main Building). The water injection will not be affected since
water will be injected to the reactor from the buffer tank which
consists of desalinated water.