*Updates are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
-Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
-At 10:11 am on December 10, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
The current water injection volume is approx 4.8 m3/h from the reactor
feed water system and approx. 2.0 m3/h from the core spray system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at
1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
-On October 28, we completed installation of the cover for the Reactor
Building in order to contain dispersion of radioactive substances.
-At 4:04 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
Unit 2 (Shut down)
-At approximately 6:00 am on March 15, an abnormal noise began emanating
from nearby Pressure Suppression Chamber and the pressure within the
chamber decreased.
-At 10:10 am on March 26, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
-At 2:59 pm on September 14, in addition to water injection from water
feeding system, we started water injection from piping of core spray
system to the reactor.
The current water injection volume is approx. 2.7 m3/h from the reactor
feed water system and approx. 6 m3/h from the core spray system.
-At 5:21 pm on May 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary
Containment Vessel.
-From 6:00 pm on October 28, we put the gas management system of the
reactor containment vessel in operation.
-At 10:46 am on December 1, we started the nitrogen injection to the
Reactor Pressure Vessel.
Unit 3 (Shut down)
-Explosive sound and white smoke were confirmed at approximately 11:01 am
on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray
system in addition to water injection by the reactor feed water system
piping arrangement.
The current water injection volume is approx 2.8 m3/h from the reactor
feed water system and approx. 5.8 m3/h from the core spray system.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary
Containment Vessel started.
-At 4:26 pm on November 30, we started operation to inject nitrogen into
the reactor pressure vessel.
Unit 4 (Outage due to regular inspection)
-At around 6 am on March 15, we confirmed the explosive sound and the
sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
-At 10:58 am on November 29, in order to decrease more salinity, we
installed Ion exchange equipment and started the operation of such
equipment.
-At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump
in order to cool the spent fuel pool.
-At 2:45 pm on July 15, we started the operation of the original Residual
Heat Removal System (System B) by its original seawater pump.
-At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 6 (Outage due to regular inspection)
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump
of Unit 6 to cool down Spent Fuel Pool.
-At 2:33 pm on September 15, we started separately cooling the reactor
through the Residual Heat Removal System and the spent fuel pool through
Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage
inside PCV.
Others
-At around 10 am on June 13, we started the operation of the circulating
seawater purification facility installed at the screen area of Unit 2 and
3.
-At 8 pm on June 17, we started operation of Water Treatment Facility
against the accumulated water. At 6:00 pm on July 2, we started the
circulating injection cooling to inject the water, which was treated by
the accumulated water treatment system, to the reactors through the
buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by
parallel operation of one line from the cesium adsorption instrument to
the decontamination instrument and the other treatment line of the cesium
adsorption instrument No.2.
-At 2:06 pm on October 7, we started to spray purified accumulated water
brought from Unit 5 and 6 continually in order to prevent dust scattering
and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea
side, in front of the existing shore protection, Units 1-4, in order to
contain marine pollution by underground water.
-At 12:25 pm on December 13, we started the re-circulating operation of
desalination facility (reverse osmosis membrane type) for the purpose of
suppression of condensed water after desalination treatment.
-At 10:00 am on December 18, during the patrol activity, a TEPCO employee
found an accumulated water in the trench located between the process main
building of Centralized Radiation Waste Treatment Facility and
Miscellaneous Solid Waste Volume Reduction Treatment Building (High
Temperature Incinerator Building). The depth of the water was estimated
to be 50 cm and the amount was to be 125 m3. The radiation dose at the
water surface was 3 mSv/h (provisional value). As no radioactive
materials have been detected during the last sampling survey of sub drain
water near the trench, the source of the accumulated water is estimated
to be the ground water or dew condensation water. After that we found
water inflow from cable duct near the ceiling of the trench by detailed
survey at site, and we recalculated the amount of the accumulated water
and it was estimated to be approx. 230 m3. And as a result of the
sampling, Cesium-134 was approx. 4.2x103 Bq/cm3, Cesium-137 was approx.
5.4x103 Bq/cm3 and Iodine-131 was below detection limit regarding the
radioactivity density of the accumulated water in the trench, and
Cesium-134 was approx. 1.3x10-1 Bq/cm3, Cesium-137 was approx. 1.2x10-1
Bq/cm3 and Iodine-131 was below detection limit regarding the inflowing
water from cable duct. We have conducted water shut-off treatment of the
trench and the groundwater level is higher than the water level in the
trench, therefore we assumed that there is no possibility of inflow of
the accumulated water in the trench to the groundwater. We will conduct
investigation continuously and monitor the water level in the trench