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Corporate Information

 
Press Release (Dec 12,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 3:00 pm, December 12)
*Updates are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down) 
-Explosive sound and white smoke were confirmed after the big quake 
 occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line. 
-At 10:11 am on December 10, in addition to water injection from water 
 feeding system, we started water injection from piping of core spray 
 system to the reactor.
 The current water injection volume is approx 4.4 m3/h from the reactor 
 feed water system and approx. 1.9 m3/h from the core spray system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at 
 1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. 
 At 10:20 pm on December 11, we stopped the alternative cooling equipment 
 for spent fuel pool, in order to conduct power source changeover work for 
 improving power supply reliability. It is scheduled to resume cooling 
 operation in the afternoon on December 12. The temperature of the pool 
 was 14 degrees at the time of suspension, and is estimated to rise for 
 approx. 3 degrees due to the suspension.
-On October 28, we completed installation of the cover for the Reactor 
 Building in order to contain dispersion of radioactive substances.
-At 4:04 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. 
Unit 2 (Shut down) 
-At approximately 6:00 am on March 15, an abnormal noise began emanating 
 from nearby Pressure Suppression Chamber and the pressure within the 
 chamber decreased. 
-At 10:10 am on March 26, we started injecting freshwater to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line. 
 At 2:59 pm on September 14, we started injecting water to the reactor 
 through core spray system water injection piping arrangement in addition 
 to the water injection through reactor feed water system piping 
 arrangement. 
 The current water injection volume is approx 2.7 m3/h from the reactor 
 feed water system and approx. 6.1 m3/h from the core spray system.
-At 5:21 pm on May 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System. 
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary 
 Containment Vessel.
-From 6:00 pm on October 28, we put the gas management system of the 
 reactor containment vessel in operation.
-At 10:46 am on December 1, we started the nitrogen injection to the 
 Reactor Pressure Vessel. 
Unit 3 (Shut down) 
-Explosive sound and white smoke were confirmed at approximately 11:01 am 
 on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor 
 and are now injecting fresh water by a motor driven pump powered by the 
 off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray 
 system in addition to water injection by the reactor feed water system 
 piping arrangement. 
 The current water injection volume is approx 2.9 m3/h from the reactor 
 feed water system and approx. 5.9 m3/h from the core spray system.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary 
 Containment Vessel started. 
-At 4:26 pm on November 30, we started operation to inject nitrogen into 
 the reactor pressure vessel. 
Unit 4 (Outage due to regular inspection) 
-At around 6 am on March 15, we confirmed the explosive sound and the 
 sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the 
 spent fuel pool by an alternative cooling equipment of the Fuel Pool 
 Cooling and Filtering System.
-At 10:58 am on November 29, in order to decrease more salinity, we 
 installed Ion exchange equipment and started the operation of such 
 equipment.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump 
 in order to cool the spent fuel pool.
-At 2:30 pm on March 20, the reactor achieved cold shutdown.
-At 2:45 pm on July 15, we started the operation of the original Residual 
 Heat Removal System (System B) by its original seawater pump.
-At this moment, we don't think there is any reactor coolant leakage 
 inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
 of Unit 6 to cool down Spent Fuel Pool.
-At 7:27 pm on March 20, the reactor achieved cold shutdown. 
-At 2:33 pm on September 15, we started separately cooling the reactor 
 through the Residual Heat Removal System and the spent fuel pool through 
 Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage 
 inside PCV. 
Others 
-At around 10 am on June 13, we started the operation of the circulating 
 seawater purification facility installed at the screen area of Unit 2 and 
 3.
-At 8 pm on June 17, we started operation of Water Treatment Facility 
 against the accumulated water. At 6:00 pm on July 2, we started the 
 circulating injection cooling to inject the water, which was treated by 
 the accumulated water treatment system, to the reactors through the 
 buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by 
 parallel operation of one line from the cesium adsorption instrument to 
 the decontamination instrument and the other treatment line of the cesium 
 adsorption instrument No.2. 
-At 2:06 pm on October 7, we started to spray purified accumulated water 
 brought from Unit 5 and 6 continually in order to prevent dust scattering 
 and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea 
 side, in front of the existing shore protection, Units 1-4, in order to 
 contain marine pollution by underground water.
-At 6:03 pm on November 30, we started transfer of the accumulated water 
 from the basement of Unit 2 turbine building to Centralized Radiation 
 Waste Treatment Facility High Temperature Incinerator Building.
-At 3:48 pm on December 11, we confirmed that the water was accumulated 
 inside the gate in the house where the water desalination equipment 
 (evaporative concentration equipment) 2 was installed. The amount of the 
 leaked water is approx. 5 litters, and the water was kept within the gate. 
 We also confirmed that the leakage has been stopped, and that it was 
 leaked from a ventilation pipe at the tank storing the seal water for the 
 evaporative concentration equipment 2B. The source of the water is the 
 filtered water (fresh water), and the radiation doses of the surface near 
 the leaked water are 0.12 mSv/h (gamma ray), and less than 1 mSv/h (beta 
 ray), which are the same level as the airborne radiation doses nearby. We 
 will investigate the cause. Since water desalination equipment (reverse 
 osmosis membrane equipment) 2-1 and 2-2 are continuously working, which 
 generate the sufficient amount of desalinated water, there is no impact 
 on the water injection to the reactors. At approx. 11:00 am on December 
 12, we confirmed that the remaining water in the hose was oozing from the 
 leakage point (the leakage amount is about 1 drop in 3 seconds). Later we 
 removed the water from the tank for the seal water and from the hose. At 
 approx. 3:00 pm on the same day, we confirmed that the water ceased to 
 ooze. 
-At 10:00 am on December 12, we started transferring of accumulated water 
 from the Turbine Building of Unit 6 to the temporary tank.
-When we cut the power of the PCV gas control system (Line A: under 
 suspension) of Unit 1 to switch the power source for the improvement work 
 of the on-site power source at approx. 10:38 am on December 12, the 
 monitoring system in the main anti-earthquake building for the same 
 system (Line B: under commissioning) was stopped. At approx. 11:30 am, we 
 confirmed on site that the system (Line B) was stopped. Later, it was 
 revealed that the power for controlling Line B comes from Line A, 
 therefore we switched the power for the control, then at 12:00 pm we 
 resumed Line B. Since Line B is normally operating after the re-start, we 
 estimate that the reason Line B went down is that the power for Line A 
 was cut. 
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