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Corporate Information

 
Press Release (Nov 27,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 3:00 pm, November 27)
Updates are underlined. 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down)  
-Explosive sound and white smoke were confirmed after the big quake
 occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
-At 3:37 pm on March 25, we started injecting freshwater to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line.
 The current water injection volume is approx 4.5m3/h from the reactor
 feed water system.
-We commenced injection of nitrogen gas into Primary Containment Vessel at
 1:31 am on April 7.
-At 11:22 am on August 10, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
  Cooling and Filtering System. 
-On October 28, we completed installation of the cover for the Reactor
 Building in order to contain dispersion of radioactive substances. 
Unit 2 (Shut down)  
-At approximately 6:00 am on March 15, an abnormal noise began emanating
 from nearby Pressure Suppression Chamber and the pressure within the
 chamber decreased. 
-At 10:10 am on March 26, we started injecting freshwater to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line. 
-At 2:59 pm on September 14, we started injecting water to the reactor
 through core spray system water injection piping arrangement in addition
 to the water injection through reactor feed water system piping
 arrangement.
 Water is currently injected at approx. 3.1m3/h through reactor feed water
 system piping arrangement, and at approx. 4.5 m3/h through core spray
 system water injection piping arrangement.
-At 5:21 pm on May 31, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System. 
-At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary
 Containment Vessel.
-From 6:00 pm on October 28, we put the gas management system of the
 reactor containment vessel in operation.
-At 11:04 am on November 6, we started operation of radioactive material
 decontamination instrument of spent fuel pool.
*As of 5:00 pm on November 26, the indicator of the gas temperature of 
 Suppression Chamber read 52.7°C, but at 11:00 pm on the day we confirmed 
 that it read "Overscaled" (digital recorder). Then, as of 5:00 am on 
 November 27, it read 102.6°C. Though the readings were not stable, as 
 there were no significant changes or variations in the temperatures of 
 the same types of 2 thermometers and the pool water in Suppression 
 Chamber, we have been investigating the causes for this event including 
 the possibility of malfunction of the measuring instruments.  
*The indicator for the inside of the Primary Containment Vessel(Drywell) 
 of Unit 2 (base line temperature of the air conditioning unit, local 
 cooling equipment) read 78.2°C as of 5:00 am on November 27 but at 6:50 
 am on the day it was confirmed that it read approximately 84°C, 
 increasing in a staircase pattern. On the other hand, it was also 
 confirmed that the temperature changes of the bottom of the Reactor 
 Pressure Vessel and the water in the pool of the Suppression Chamber were 
 smaller than that of the inside of the Primary Containment Vessel 
 (Drywell) and that there was no significant change in the temperature. 
 Now we have been decreasing the flow rate of water injection as shown in 
 the below and therefore it is expected that the temperature inside the 
 Primary Containment Vessel will rise, but, as the line of which 
 temperature rose in a staircase pattern was only one line of the five 
 lines and the rest of the lines did not show the same changes, we have 
 been investigating the causes for this event, including the possibility 
 of malfunction of the measuring instruments. We will continue to monitor 
 the temperatures. 
 ·At 7:11 pm on November 24, we adjusted the flow rate of water injection 
   from Core Spray System from approx. 7.2 m3/h to approx. 5.6m3/h (for 
   feed water system, the flow rate is kept at 2.9 m3/h). 
 ·On November 26 (from 10:18 am to 11:02 am), we adjusted the flow rate  
   from Core Spray System from approx. 5.5 m3/h to approx. 4.5m3/h (for  
   feed water system, the flow rate is kept at 3.0 m3/h). 
* At 2:54 pm on November 25, we started transferring accumulated water from
  Unit 1 T/B basement to Unit 2 T/B basement. At 9:38 am on November 27,  
  we stopped transferring it. 
Unit 3 (Shut down)  
-Explosive sound and white smoke were confirmed at approximately 11:01 am
 on March 14. It was assumed to be hydrogen explosion.
-At 6:02 pm on March 25, we started injecting fresh water to the reactor
 and are now injecting fresh water by a motor driven pump powered by the
 off-site transmission line.
-At 2:58 pm on September 1, we started water injection by core spray
 system in addition to water injection by the reactor feed water system
 piping arrangement. 
 Water is currently injected at approx. 1.9 m3/h through reactor feed
 water system piping arrangement, and at approx. 6.0 m3/h through core
 spray system water injection piping arrangement.
-At 7:47 pm on June 30, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System.
-At 8:01 pm on July 14, injection of nitrogen gas into the Primary
 Containment Vessel started. 
Unit 4 (Outage due to regular inspection)  
-At around 6 am on March 15, we confirmed the explosive sound and the
 sustained damage around the 5th floor rooftop area of Reactor Building.
-At 12:44 pm on July 31, we started cyclic cooling for the water in the
 spent fuel pool by an alternative cooling equipment of the Fuel Pool
 Cooling and Filtering System.
-At 11:34 am on August 20, we started an operation of desalination
 equipment in the spent fuel pool.
-At this moment, we don't think there is any reactor coolant leakage
 inside the primary containment vessel. 
Unit 5 (Outage due to regular inspection)  
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 5:00 am on March 19, we started the Residual Heat Removal System Pump
 in order to cool the spent fuel pool.
-At 2:30 pm on March 20, the reactor achieved cold shutdown.
-At 2:45 pm on July 15, we started the operation of the original Residual
 Heat Removal System (System B) by its original seawater pump.
-At this moment, we don't think there is any reactor coolant leakage
 inside the primary containment vessel. 
Unit 6 (Outage due to regular inspection)  
-Sufficient level of reactor coolant to ensure safety is maintained.
-At 10:14 pm on March 19, we started the Residual Heat Removal System Pump
 of Unit 6 to cool down Spent Fuel Pool.
-At 7:27 pm on March 20, the reactor achieved cold shutdown. 
-At 2:33 pm on September 15, we started separately cooling the reactor
 through the Residual Heat Removal System and the spent fuel pool through
 Equipment Cooling Water System and Fuel Pool Cooling System.
-At this moment, we do not think there is any reactor coolant leakage
 inside PCV. 
Others  
-At around 10 am on June 13, we started the operation of the circulating
 seawater purification facility installed at the screen area of Unit 2 and 3.
-At 8 pm on June 17, we started operation of Water Treatment Facility
 against the accumulated water. At 6:00 pm on July 2, we started the
 circulating injection cooling to inject the water, which was treated by
 the accumulated water treatment system, to the reactors through the
 buffer tank.
-At 7:41 pm on August 19, we started treatment of accumulated water by
 parallel operation of one line from the cesium adsorption instrument to
 the decontamination instrument and the other treatment line of the cesium
 adsorption instrument No.2. 
-At 2:06 pm on October 7, we started to spray purified accumulated water
 brought from Unit 5 and 6 continually in order to prevent dust scattering
 and potential fire outbreaks from the cut down trees.
-On October 28, we started installation of the water proof wall at the sea
 side, in front of the existing shore protection, Units 1-4, in order to
 contain marine pollution by underground water.
-At 9:10 am on November 10, we started transfer of accumulated water from
 the basement of Unit 2 turbine building to Centralized Radiation Waste
 Treatment Facility High Temperature Incinerator Building.
-At 9:25 am on November 15, we started transfer of accumulated water from
 basement of Unit 3 turbine building to Centralized Radiation Waste
 Treatment Facility Building. 
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