*Updates are underlined
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- At 3:37 pm on March 25, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
The current water injection volume is approx 7.8 m3/h from the reactor
feed water system.
- We commenced injection of nitrogen gas into Primary Containment Vessel
at 1:31 am on April 7.
- At 11:22 am on August 10, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- On October 28, we completed installation of the cover for the Reactor
Building in order to contain dispersion of radioactive substances.
Unit 2 (Shut down)
- At approximately 6:00 am on March 15, an abnormal noise began emanating
from nearby Pressure Suppression Chamber and the pressure within the
chamber decreased.
- At 10:10 am on March 26, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:59 pm on September 14, we started injecting water to the reactor
through core spray system water injection piping arrangement in addition
to the water injection through reactor feed water system piping
arrangement.
Water is currently injected at approx. 3 m3/h through reactor feed water
system piping arrangement, and at approx. 7.3 m3/h through core spray
system water injection piping arrangement.
- At 5:21 pm on May 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the
Primary Containment Vessel.
- From 6:00 pm on October 28, we put the gas management system of the
reactor containment vessel in operation.
- At 11:04 am on November 6, we started operation of radioactive material
decontamination instrument of spent fuel pool.
Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01 am
on March 14. It was assumed to be hydrogen explosion.
- At 6:02 pm on March 25, we started injecting fresh water to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- At 2:58 pm on September 1, we started water injection by core spray
system in addition to water injection by the reactor feed water system
piping arrangement.
Water is currently injected at approx. 2.3 m3/h through reactor feed
water system piping arrangement, and at approx. 8 m3/h through core
spray system water injection piping arrangement.
- At 7:47 pm on June 30, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary
Containment Vessel started.
- At 2:30 pm on November 7, we suspended the alternative cooling in order
to clear clogs in the primary strainer resulted from reverse cleaning,
as a countermeasure against the alarm suction pressure decrease of
alternative primary coolant system pump in spent fuel pool of Unit 3 at
Fukushima Daiichi Nuclear Power Station (water temperature of spent fuel
pool as of suspension: approx. 24.8°C). After finishing the reverse
cleaning of the primary strainer, then, at 7:17 pm on the same day we
restarted the alternative cooling (water temperature of spent fuel pool
as of restart: approx. 22.5°C *It is supposed that water temperature as
of restart became lower than that as of suspension because water in
skimmer surge tank was cooled down by outside air.
Unit 4 (Outage due to regular inspection)
- At around 6 am on March 15, we confirmed the explosive sound and the
sustained damage around the 5th floor rooftop area of Reactor Building.
- At 12:44 pm on July 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 11:34 am on August 20, we started an operation of desalination
equipment in the spent fuel pool.
- At 12:25 am on November 8, RO membrane unit of desalting facility in
spent fuel pool, Unit 4 automatically stopped due to the alarm
indicating leakage. Responding to the alarm, we confirmed that all the
isolation valves of each unit were closed by the interlocks. Also,
considering that all the spots at leakage risk were equipped with
receiving pans which would be able to store all of the liquid in the
unit, we judged that further deterioration of leakage or leakage to
outside of the unit was unlikely. We will check the site and situation
in the future. The operation of circulating cooling system has been
continued.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System Pump
in order to cool the spent fuel pool.
- At 2:30 pm on March 20, the reactor achieved cold shutdown.
- At 2:45 pm on July 15, we started the operation of the original Residual
Heat Removal System (System B) by its original seawater pump.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System
Pump of Unit 6 to cool down Spent Fuel Pool.
- At 7:27 pm on March 20, the reactor achieved cold shutdown.
- At 2:33 pm on September 15, we started separately cooling the reactor
through the Residual Heat Removal System and the spent fuel pool through
Equipment Cooling Water System and Fuel Pool Cooling System.
- At this time, we don't think there is any reactor coolant leakage inside
the primary containment vessel.
Others
- At around 10 am on June 13, we started the operation of the circulating
seawater purification facility installed at the screen area of Unit 2
and 3.
- At 8 pm on June 17, we started operation of Water Treatment Facility
against the accumulated water. At 6:00 pm on July 2, we started the
circulating injection cooling to inject the water, which was treated by
the accumulated water treatment system, to the reactors through the
buffer tank.
- At 7:41 pm on August 19, we started treatment of accumulated water by
parallel operation of one line from the cesium adsorption instrument to
the decontamination instrument and the other treatment line of the
cesium adsorption instrument No.2.
- At 2:06 pm on October 7, we started to spray purified accumulated water
brought from Unit 5 and 6 continually in order to prevent dust
scattering and potential fire outbreaks from the cut down trees.
- On October 28, we started installation of the water proof wall at the
sea side, in front of the existing shore protection, Units 1-4, in order
to contain marine pollution by underground water.
- At 10:11 am on November 2, we started transferring the accumulated water
from the basement of the Unit 3 turbine building to the High Temperature
Incinerator Building of the Centralized Radiation Waste Treatment
Facility.
- At 9:38 am on November 4, we started transferring the accumulated water
from the basement of the Unit 2 turbine building to Centralized
Radiation Waste Treatment Facility.
- At around 11:00 am on November 6, since partner companies' workers who
went on patrol found that the boiler of evaporative concentration
apparatus stopped, we stopped operation of the apparatus 3B and 3C.
Since the operation panel on the site alerted "Very low water level in
boiler supply water tank", we assumed that the boiler stopped due to
this reason. After that, we conducted investigation of the cause of
decrease of supply tank water level. When we started a backup pump for
transfer of boiler supply water, the alert stopped. Therefore we judged
that one pump was troubled.
At 2:55 pm on November 7, we started another boiler by using a spare
water transfer pump for boiler. Then, we started evaporative
concentration apparatus 3B at 5:24 pm and 3C at 6 pm. Causes of the
trouble of the water transfer pump for boiler are still under
investigation. At 2:24 am on November 8, we manually stopped the boiler
of evaporative concentration apparatus in the water desalinations since
alarm worked and indicated decrease of water level in boiler water
supply tank at 2:20 am. Then, we stopped evaporative concentration
apparatus 3B at 2:28 am ad 3C at 2:31 am. Although all the evaporative
concentration apparatus stopped, water treatment by the water
desalinations (RO membrane system) and water injection to the reactors
have been continued. Causes will be investigated in the future.