*Updates are underlined.
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down.
Unit 1 (Shut down)
- Explosive sound and white smoke were confirmed after the big quake
occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- From 3:37 pm on March 25, we started injecting freshwater by a motor
driven pump which is now powered by the off-site transmission line.
- As decrease of water injection into the reactor was confirmed at 5:40 pm
on September 11, we adjusted the flow control through reactor feed water
system piping arrangement. It was raised to approx. 3.8 m3/h.
Water is currently injected at approx. 3.8 m3/h through reactor feed
water system piping arrangement.
- We commenced injection of nitrogen gas into Primary Containment Vessel at
1:31am on April 7.
- At 9:00 am on August 10, we started to assemble steel frame for the
Reactor Building Cover.
- At 11:22 pm on August 10, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
Unit 2 (Shut down)
- At approximately 6:00 am on March 15, an abnormal noise began emanating
from nearby Pressure Suppression Chamber and the pressure within the
chamber decreased.
- From 10:10 am on March 26, we started injecting freshwater to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- As decrease of water injection into the reactor was confirmed at 5:40 pm
on September 11, we adjusted the flow control through reactor feed water
system piping arrangement. It was raised to approx. 3.8 m3/h.
Water is currently injected at approx. 3.7 m3/h through reactor feed water
system piping arrangement.
- From 5:21 pm on May 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary
Containment Vessel.
Unit 3 (Shut down)
- Explosive sound and white smoke were confirmed at approximately 11:01am
on March 14. It was assumed to be hydrogen explosion.
- From 6:02 pm on March 25, we started injecting fresh water to the reactor
and are now injecting fresh water by a motor driven pump powered by the
off-site transmission line.
- From 2:58 pm on September 1, we started water injection by core spray
system in addition to water injection by the reactor feed water system
piping arrangement.
- From 2:01 pm on September 12, we adjusted the flow control through
reactor feed water system piping arrangement. It was reduced to approx.
4 m3/h.
Water is currently injected at approx. 4 m3/h through reactor feed water
system piping arrangement, and at approx. 3 m3/h through core spray
system.
- From 7:47 pm on June 30, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary
Containment Vessel started.
Unit 4 (Outage due to regular inspection)
- At approximately 6 am on March 15, we confirmed the explosive sound and
the sustained damage around the 5th floor rooftop area of Reactor
Building.
- From 0:44 pm on July 31, we started cyclic cooling for the water in the
spent fuel pool by an alternative cooling equipment of the Fuel Pool
Cooling and Filtering System.
- From 11:34 am on August 20, we started an operation of desalination
equipment in the spent fuel pool.
- At this moment, we don't think there is any reactor coolant leakage
inside the primary containment vessel.
Unit 5 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System Pump
in order to cool the spent fuel pool.
- At 2:30 pm on March 20, the reactor achieved cold shutdown.
- At 2:45 pm on July 15, we started the operation of the original Residual
Heat Removal System (System B) by its original seawater pump.
- At this time, we don't think there is any reactor coolant leakage inside
the primary containment vessel.
Unit 6 (Outage due to regular inspection)
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System Pump
of Unit 6 to cool down Spent Fuel Pool.
- At 7:27 pm on March 20, the reactor achieved cold shutdown.
- At this time, we don't think there is any reactor coolant leakage inside
the primary containment vessel.
- At 3:12 pm on September 10, we started cooling the spent fuel pool
through the Residual Heat Removal System A using the seawater pump C. We
will conduct cooling the reactor and the spent fuel pool by turn through
the System A.
Others
- At around 10 am on June 13, we started the operation of the circulating
seawater purification facility installed at the screen area of Unit 2 and 3.
- At 8:00 pm on June 17, we started operation of Water Treatment Facility
against the accumulated water. At 6:00 pm on July 2, we started the
circulating injection cooling to inject the water, which was treated by
the accumulated water treatment system, to the reactors through the
buffer tank.
- At 7:41 pm on August 19, we started treatment of accumulated water by
parallel operation of one line from the cesium adsorption instrument to
the decontamination instrument and the other treatment line of the 2nd
cesium adsorption instrument.
- At 9:39 am on August 30, we started transferring accumulated water from
the turbine building of Unit 2 to Process Main Building of Centralized
Radiation Waste Treatment Facility.
- At 9:30 am on September 8, we started transferring accumulated water from
the turbine building of Unit 3 to Process Main Building of Centralized
Radiation Waste Treatment Facility. From 10:00 am on September 11, we
changed to transfer to the High Temperature Incinerator Building of
Centralized Radiation Waste Treatment Facility.
- At approximately 10:00 am on September 12, we confirmed that indication
of a movable monitoring post was unreadable. The post had monitored the
dose rate at the main gate of the Power plant. The data transmission was
resumed at 10:20 am on September 12. We are watching it carefully.
- At 11:30 am on September 12, we started transferring accumulated water
from the turbine building of Unit 6 to the temporary tank.