search



Corporate Information

 
Press Release (Aug 18,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 4:00 pm, Aug. 18)
*New items are underlined 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
- Explosive sound and white smoke were confirmed after the big quake 
  occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- At approximately 2:30 am on March 23, seawater injection to the reactor 
  through the reactor feed water system was initiated.
- From 3:37 pm on March 25, we started injecting freshwater by a motor 
  driven pump which is now powered by the off-site transmission line. 
  Water is currently injected at approx. 3.8 m3/h through reactor feed 
  water system piping arrangement.
- We commenced injection of nitrogen gas into Primary Containment Vessel 
  at 1:31am on April 7.
- At 9:00 am on August 10, we started to assemble steel frame for the 
  Reactor Building Cover. 
Unit 2 (Shut down) 
- At approximately 6:00 am on March 15, an abnormal noise began emanating 
  from nearby Pressure Suppression Chamber and the pressure within the 
  chamber decreased. 
- From 10:10 am on March 26, we started injecting freshwater to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line.
- At 3:46 pm on August 17, as we confirmed the decrease in the rate of 
  water injection to the reactor, we adjusted the rate of water injection 
  from feed water system piping arrangement at approx. 3.8 m3/h.
  Water is currently injected at approx. 3.8 m3/h through reactor feed 
  water system piping arrangement.
- At 8:06 pm on June 28, we started injecting nitrogen gas into the Primary 
  Containment Vessel. 
Unit 3 (Shut down) 
- Explosive sound and white smoke were confirmed at approximately 11:01am 
  on March 14. It was assumed to be hydrogen explosion.
- From 6:02 pm on March 25, we started injecting fresh water to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line.
  Water is currently injected at approx. 9.1 m3/h through reactor feed 
  water system piping arrangement.
- At 7:38 am on August 18, we switched water injection line to the reactor 
  from the line which is using a motor driven pump powered by the off-site 
  transmission line to the line which is using a motor driven pump powered 
  by emergency diesel generator. At 12:20 pm on the same day, we installed 
  flow regulating valve to the pipes of water injection line and we switched 
  water injection line to original line. At 12:27 pm on the same day, we 
  adjusted the rate of injecting water to the reactor at approx. 8 m3/h. 
- Water is currently injected at approx. 8 m3/h through reactor feed water 
  system piping arrangement.
- At 8:01 pm on July 14, injection of nitrogen gas into the Primary 
  Containment Vessel started. 
Unit 4 (Outage due to regular inspection) 
- At approximately 6 am on March 15, we confirmed the explosive sound and 
  the sustained damage around the 5th floor rooftop area of Reactor Building.
- At this moment, we don't think there is any reactor coolant leakage inside 
  the primary containment vessel. 
Unit 5 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5 am on March 19, we started the Residual Heat Removal System Pump in 
  order to cool the spent fuel pool.
- At 2:30 pm on March 20, the reactor achieved cold shutdown.
- At 2:45 pm on July 15, we started the operation of the original Residual 
  Heat Removal System Pump (B).
- At this time, we don't think there is any reactor coolant leakage inside 
  the primary containment vessel. 
Unit 6 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
  of Unit 6 to cool down Spent Fuel Pool.
- At 7:27 pm on March 20, the reactor achieved cold shutdown. 
- At this time, we don't think there is any reactor coolant leakage inside 
  the primary containment vessel. 
Operation for cooling the Spent Fuel Pools 
- At 5:21 pm on May 31, we started cyclic cooling of Spent Fuel Pool of 
  Unit 2 by using alternative cooling system of the Pool's cooling and 
  filtering system.
- At 7:47 pm on June 30, we started cyclic cooling of Spent Fuel Pool of 
  Unit 3 by using alternative cooling system of the Pool's cooling and 
  filtering system. And from 11:06 am to 1:00 pm on August 18, we also 
  injected hydrazine (corrosion inhibitor). 
- At 12:44 pm on July 31, we started cyclic cooling of Spent Fuel Pool of 
  Unit 4 by using alternative cooling system of the Pool's cooling and 
  filtering system.
- At 11:22 am on Aug 10, we started cyclic cooling of Spent Fuel Pool of 
  Unit 1 by using alternative cooling system of the Pool's cooling and 
  filtering system. 
Others 
- At 11:00 am on May 10, we started transferring accumulated water from 
  the underground level of reactor building to the radiation waste treatment 
  facility of Unit 6.
- At around 10 am on June 13, we started the operation of the circulating 
  seawater purification facility installed at the screen area of Unit 2 
  and 3.
- At 8:00 pm on June 17, we started operation of Water Treatment Facility 
  against the accumulated water. 
- At 6:00 pm on July 2, we started the circulating injection cooling to 
  inject the water, which was treated by the accumulated water treatment 
  system, to the reactors through the buffer tank.
- At 12:04 pm on August 16, we stopped the operation of water treatment 
  facility for the combined test of existing facilities and the second 
  cesium adsorption equipment which was additionally installed. At 2:43 pm 
  on August 18, we started the operation of the water treatment system. 
  After that, 3:50 pm on the same day, we stopped the test and resumed 
  water treatment. 
- At 10:00 am, we started transferring accumulated water from the turbine 
  building of Unit 6 to a temporary tank.
- From approx 2:30 pm on August 18, the instrument reading of transportable 
  monitoring post became unreadable. After that, on approx 4:00 pm on the 
  same day, we confirmed the monitoring post indicated normal instrument 
  reading. We will continue monitoring carefully. 
back to page top


to TOP