search



Corporate Information

 
Press Release (Jun 27,2011)
Plant Status of Fukushima Daiichi Nuclear Power Station (as of 10:00 pm, June 27)
 
*No updates in this issue 
All 6 units of Fukushima Daiichi Nuclear Power Station have been shut down. 
Unit 1 (Shut down) 
- Explosive sound and white smoke were confirmed after the big quake 
  occurred at 3:36 pm on March 12. It was assumed to be hydrogen explosion.
- At approximately 2:30 am on March 23, seawater injection to the reactor 
  through the reactor feed water system was initiated.
- From 3:37 pm on March 25, we started injecting freshwater by a motor 
  driven pump which is now powered by the off-site transmission line. Water 
  is currently injected at approx. 3.5m3/h through reactor feed water 
  system piping arrangement.
- As it was suspected that hydrogen gas had been accumulated inside Primary 
  Containment Vessel, in order to prevent increase in density of oxygen, we 
  commenced the valve opening operation concerning injection of nitrogen 
  gas into the primary containment vessel at 10:30 pm on April 6 and 
  commenced injection at 1:31am April 7. 
Unit 2 (Shut down) 
- At approximately 6:00 am on March 15, an abnormal noise began emanating 
  from nearby Pressure Suppression Chamber and the pressure within the 
  chamber decreased. 
- From 10:10 am on March 26, we started injecting freshwater to the reactor 
  and are now injecting freshwater by a motor driven pump powered by the 
  off-site transmission line. 
  At 6:27 pm on June 23, we changed the water injection line so that we can 
  inject water to Unit 1 and 2 by the motor driven pump for Unit 1 and 
  stopped the motor driven pump for Unit 2. 
  Water is currently injected at approx. 3.5m3/h through reactor feed water 
  system piping arrangement. 
Unit 3 (Shut down) 
- Explosive sound and white smoke were confirmed at approximately 11:01am 
  on March 14. It was assumed to be hydrogen explosion.
- From 6:02 pm on March 25, we started injecting fresh water to the reactor 
  and are now injecting fresh water by a motor driven pump powered by the 
  off-site transmission line.
  Water is currently injected at approx. 9 m3/h through reactor feed water 
  system piping arrangement. 
Unit 4 (Outage due to regular inspection) 
- At approximately 6:00 am on March 15, we confirmed the explosive sound 
  and the sustained damage around the 5th floor rooftop area of Reactor 
  Building.
- At this moment, we do not consider any reactor coolant leakage inside the 
  primary containment vessel has occurred. 
Unit 5 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 5:00 am on March 19, we started the Residual Heat Removal System Pump 
  (C) in order to cool the spent fuel pool.
- At 2:30 pm on March 20, the reactor achieved cold shutdown. 
- At this moment, we do not consider any reactor coolant leakage inside the 
  primary containment vessel has occurred. 
Unit 6 (Outage due to regular inspection) 
- Sufficient level of reactor coolant to ensure safety is maintained.
- At 10:14 pm on March 19, we started the Residual Heat Removal System Pump 
  (B) of Unit 6 in order to cool the spent fuel pool.
- At 7:27 pm on March 20, the reactor achieved cold shutdown.  
- At this moment, we do not consider any reactor coolant leakage inside the 
  primary containment vessel has occurred. 
Operation for cooling the spent fuel pools 
- At 5:21 pm on May 31, we started cyclic cooling of the spent fuel pool in 
  Unit 2 using alternative cooling system for fuel pool cooling and 
  filtering system. 
- At 4:35 pm on June 24, We started the cooling of the spent fuel pool by 
  the pump of the Fuel Pool Cooling and Filtering System.
- We will continuously conduct further water spray depending on the 
  conditions of spent fuel pools, if needed. 
Others 
- At 1:30 pm on April 26, we started spraying the dust inhibitor inside the 
  site. 
- At 11:00 am on May 10, we started transferring accumulated water from the 
  underground level of reactor building to the radiation waste treatment 
  facility of Unit 6.
- At approximately 10:00 am on June 13, we started the operation of the 
  circulating seawater purification facility installed at the screen area 
  of Unit 2 and 3.
- From 8:00 pm on June17, we started operation of water treatment of 
  accumulated water at accumulated water treatment facility. 
- At 3:32 pm on June 21, we started transferring accumulated water in 
  turbine building of Unit 3 to central waste treatment facility building.
- At 9:56 am on June 22, we started transferring accumulated water in 
  turbine building of Unit 2 to central waste treatment facility building.
- We will continue to take all measures to ensure the safety and to 
  continue monitoring the surrounding environment around the power station. 
back to page top


to TOP